NTSB Final Report: Fred L Wellman CH 750 Cruzer | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-11.17.25

AirborneNextGen-
11.11.25

Airborne-Unlimited-11.12.25

Airborne-FltTraining-11.13.25

AirborneUnlimited-11.14.25

LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Mon, Nov 17, 2025

NTSB Final Report: Fred L Wellman CH 750 Cruzer

About 5ft Above Ground Level, The Airplane Stalled, And The Left Wing Dropped

Location: Medina, Ohio Accident Number: ERA25LA219
Date & Time: June 5, 2025, 09:00 Local Registration: N75FW
Aircraft: Fred L Wellman CH 750 Cruzer Aircraft Damage: Substantial
Defining Event: Loss of control in flight Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Flight test

Analysis: The pilot reported that this flight was conducted as part of phase 1 flight testing of the newly constructed experimental amateur-built airplane. The pilot stated that he had watched a video from the airplane kit manufacturer on “factory takeoff,” which suggested keeping the control stick slightly aft of neutral and applying partial power. During the accident takeoff, he tried the method described by the video and when the airplane lifted off, it was too slow. About 5ft above ground level, the airplane stalled, and the left wing dropped. The airplane impacted to the left of the runway and continued into a ditch and an area of brush, resulting in substantial damage to the left wing. The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s failure to maintain control of the airplane during takeoff, which resulted in a runway excursion.

FMI: www.ntsb.gov

Advertisement

More News

Classic Aero-TV: Extra Aircraft Announces the Extra 330SX

From 2023 (YouTube Edition): An Even Faster Rolling Extra! Jim Campbell joined General Manager of Extra Aircraft Duncan Koerbel at AirVenture 2023 to talk about what’s up and>[...]

Aero-News: Quote of the Day (11.15.25)

“Receiving our Permit to Fly and starting Phase 4 marks a defining moment for Vertical Aerospace. Our team has spent months verifying every core system under close regulatory>[...]

ANN's Daily Aero-Term (11.15.25): Middle Marker

Middle Marker A marker beacon that defines a point along the glideslope of an ILS normally located at or near the point of decision height (ILS Category I). It is keyed to transmit>[...]

NTSB Final Report: Lancair 320

The Experienced Pilot Chose To Operate In Instrument Meteorological Conditions Without An Instrument Flight Rules Clearance Analysis: The airplane was operated on a personal cross->[...]

Airborne 11.14.25: Last DC-8 Retires, Boeing Recovery, Teeny Trig TXP

Also: ATI Strike Prep, Spirit Still Troubled, New CubCrafters Dealership, A-29 Super Tucano Samaritan’s Purse is officially moving its historic Douglas DC-8 cargo jet into re>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC