USAF: F-16 Downed by Fuel Leak/Fire | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-12.08.25

AirborneNextGen-
12.09.25

Airborne-Unlimited-12.10.25

Airborne-AffordableFlyers-12.11.25

AirborneUnlimited-12.12.25

AFE 2025 LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Fri, Nov 25, 2005

USAF: F-16 Downed by Fuel Leak/Fire

A fuel leak and fire caused an F-16 Fighting Falcon landing at Lamar Airport, Colo., June 28 to leave the runway and crash, according to the Air Force.

The pilot ejected from the aircraft and suffered minor injuries. There was no private property destroyed, and the airport sustained minor damage. The crash destroyed the $19-million aircraft from the Colorado Air National Guard's 140th Wing at Buckley Air Force Base, Colo.

An improperly installed engine augmenter fan manifold caused the fuel leak, according to the Air Force accident investigation board report. The part supplies fuel to the rear section of the engine when it is on afterburner.

The fire damaged the aircraft's engine nozzle, speed brakes and flight controls, and rendered one of the channels of the left brake inoperative. The pilot flew a simulated flameout approach into the airport, but the broken brake caused an uncontrollable drift to the right during landing. When the pilot realized he could not prevent the aircraft from leaving the runway, he successfully ejected.

Investigators determined there is substantial evidence the failure to troubleshoot the damaged aircraft systems -- and the inadvertent movement of the brake channel switch -- did not allow the pilot to stop the aircraft on the runway.

FMI: www.af.mil

Advertisement

More News

ANN's Daily Aero-Term (12.13.25): Light Gun

Light Gun A handheld directional light signaling device which emits a brilliant narrow beam of white, green, or red light as selected by the tower controller. The color and type of>[...]

Aero-News: Quote of the Day (12.13.25)

“We have performed extensive ground testing by comparing warm up times, full power tethered pulls, and overall temperatures in 100 degree environments against other aircraft >[...]

NTSB Final Report: Gippsland GA-8

While Taxiing To Parking The Right Landing Gear Leg Collapsed, Resulting In Substantial Damage Analysis: The pilot made a normal approach with full flaps and landed on the runway. >[...]

Classic Aero-TV: Historically Unique -- Marlin Horst's Exquisite Fairchild 71

From 2014 (YouTube Edition): Exotic Rebuild Reveals Aerial Work Of Art During EAA AirVenture 2014, ANN's Michael Maya Charles took the time to get a history lesson about a great ai>[...]

Airborne 12.12.25: Global 8000, Korea Pilot Honors, AV-30 Update

Also: Project Talon, McFarlane Acquisition, Sky-Tec Service, JPL Earth Helo Tests Bombardier has earned a round of applause from the business aviation community, celebrating the fo>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC