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Thu, Sep 28, 2023

NTSB Final Report: Dwyer Michael D Q Aircraft

The Pilot Had Modified The Pull Starter Motor From Its Original Design

Location: Spring Hill, Florida Accident Number: ERA22LA159
Date & Time: March 17, 2022, 11:30 Local Registration: N3QP
Aircraft: Dwyer Michael D Q Aircraft Damage: Destroyed
Defining Event: Loss of engine power (partial) Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The pilot was also the owner and builder of the experimental amateur-built airplane. While returning to the airport after a local flight, the engine lost oil pressure, so the pilot diverted toward the nearest airport. The engine then began to run roughly and lost partial power. The airplane was not able to glide to the runway and collided with a ditch in a field during the forced landing. The pilot described that his postaccident examination of the engine revealed that the pinion gear on the pull starter motor fractured into several pieces that entered the accessory gear case, likely seizing the oil pump.

About 4 years and 100 flight hours before the accident, the pilot had modified the pull starter motor from its original design so that the motor would fit in the airplane. Postaccident metallurgical examination found that the pull starter motor’s pivot lever was shortened. The pivot lever arm was designed to move the starter clutch and engage the pinion (small) gear to the crankshaft gear. The pinion gear teeth displayed indentations in their surfaces that indicated that they were only partially engaged to the crankshaft gear when the starter was being operated, a condition which was likely the result of the shortened pivot lever. This ultimately resulted in increased stress on the gear teeth during engine start and the subsequent failure of the gear in overstress. The liberated gear teeth likely damaged and seized the engine oil pump, and resulted in the partial loss of engine power.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s improper modification of the pull starter motor, which resulted in its failure and the subsequent loss of engine power.

FMI: www.ntsb.gov

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