Investigation Of An Accident Revealed A Failed Pushrod Assembly
The FAA has issued an emergency AD prompted by an accident involving a Sikorsky Aircraft Corporation Model S-76C helicopter. During preliminary investigation, a failed servo input control pushrod (pushrod) assembly was identified. Separation of the pushrod tube and the control rod end with bearing was found.
The EAD requires inspecting the main rotor (M/R) forward, aft, and lateral pushrod assemblies, the tail rotor (T/R) pushrod assembly, and the jamnuts, and applying slippage marks across the pushrod tubes and jamnuts. These EAD actions are intended to prevent loss of M/R or T/R flight control and subsequent loss of control of the helicopter.
The FAA issued the EAD after evaluating all the relevant information and determining the unsafe condition described previously is likely to exist or develop in other products of these same type designs.
Sikorsky issued Alert Service Bulletin No. 76-67-57, Basic Issue, dated September 10, 2015 (ASB), which specifies a one-time inspection of the M/R forward, aft, and lateral pushrod assemblies, the T/R pushrod assembly, and the jamnuts for proper installation, condition, and security. If a pushrod or jamnut does not meet criteria specified in the inspection, the ASB specifies replacing the assembly. The ASB also specifies applying two slippage marks across each M/R and T/R pushrod tube and jamnut. Further, the ASB references the applicable maintenance manual for a new recurring inspection of the slippage marks.
The EAD requires, within five hours time-in-service, inspecting each M/R and T/R pushrod assembly by inspecting the position of the control rod end in the pushrod tube. If the lockwire passes through the inspection hole, this EAD requires replacing the pushrod assembly. If the lockwire does not pass through the inspection hole, this EAD requires inspecting the jamnut to determine seating position against the pushrod and whether the jamnut can be turned with finger pressure. If the jamnut is not seated against the pushrod or is loose, this EAD requires replacing the pushrod assembly.
The EAD also requires, both for those pushrod assemblies that are replaced and for those that pass the inspections, applying two slippage marks across each M/R and T/R pushrod tube and jamnut.
The FAA says it considers this EAD to be an interim action as the accident investigation is ongoing. If additional action is later identified, the agency says it might consider further rulemaking.