NTSB Final Report: Cessna 150 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-11.10.25

AirborneNextGen-
11.11.25

Airborne-Unlimited-11.12.25

Airborne-Unlimited-11.06.25

AirborneUnlimited-11.07.25

LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Wed, May 08, 2024

NTSB Final Report: Cessna 150

(FAA) Inspector Observed That Both Fuel Tanks Were Intact And That Only A Minimal Amount Of Fuel Remained In Each

Location: Dunnellon, Florida Accident Number: ERA24LA117
Date & Time: February 20, 2024, 12:38 Local Registration: N8158F
Aircraft: Cessna 150 Aircraft Damage: Substantial
Defining Event: Fuel exhaustion Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: According to the pilot, approximately 8 miles from the destination airport, and while flying at 2,000 ft mean sea level, the engine experienced a total loss of power. The pilot attempted to restart the engine but was unsuccessful. The pilot subsequently conducted a forced landing to a blueberry field impacting several sprinkler heads, which resulted in substantial damage to both wings.

The pilot stated that during his preflight inspection, a calibrated fuel dipping stick for the accident airplane make and model was not available, so the pilot “took a look down” into the fuel tanks and was relying on the instrument panel-mounted fuel gauges to determine the quantity of fuel in the airplane. The gauges read about ½ full for both tanks and the pilot felt confident that was sufficient for the planned 23-minute flight. 

A Federal Aviation Administration inspector examined the airplane after the accident. The inspector observed that both fuel tanks were intact and that only a minimal amount of fuel remained in each. The inspector also noted that the fuel gauges in the instrument panel read “at E on the left tank and just above E on the right tank.” Based on this information, it is most likely that the pilot inaccurately determined the amount of fuel available for the flight prior to departure, which subsequently resulted in fuel exhaustion and a total loss of engine power.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s inadequate preflight fuel planning, which resulted in fuel exhaustion and a subsequent total loss of engine power.

FMI: www.ntsb.gov


Advertisement

More News

NBAA Responds To GA/BA Operational Restrictions

Bolen Issues Statement Reinforcing Need To Reopen Government The National Business Aviation Association’s President and CEO issued the statement below in response to further >[...]

Boeing Deliveries Surge to Pre-Pandemic Levels

Output May Reach Its Best Since 2018 Despite Trailing Behind Airbus Boeing delivered 53 jets in October, bringing its 2025 total to 493 aircraft and marking its strongest output si>[...]

Spirit Forecasts Financial Turbulence

Low-Cost Airline Admits “Substantial Doubt” It Can Stay Airborne Spirit Airlines has once again found itself in financial trouble, this time less than a year after clai>[...]

Singapore Adds a Price Tag to Going Green

Travelers Leaving Changi Will Soon Pay for Sustainable Fuel Starting April 2026, passengers flying out of Singapore will find a new fee tucked into their tickets: a Sustainable Avi>[...]

NTSB Final Report: Arlie L Raber III Challenger 1

Pilot Was Having Difficulty Controlling The Airplane’S Rudder Pedals Due To His Physical Stature Analysis: The pilot was having difficulty controlling the airplane’s ru>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC