NTSB: NWA Flight 74 Crew Thought Gear Was Down | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-SpecialEpisode-12.15.25

AirborneNextGen-
12.16.25

Airborne-Unlimited-12.10.25

Airborne-AffordableFlyers-12.11.25

AirborneUnlimited-12.12.25

AFE 2025 LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Mon, Dec 22, 2008

NTSB: NWA Flight 74 Crew Thought Gear Was Down

Faulty Nose Gear Door Actuator Examined

The National Transportation Safety Board has released an updated factual report on the Northwest Airlines Flight 74 landing accident at Guam International Airport (GUM) on August 19, 2005.

As ANN reported, the NWA Boeing 747-200 experienced trouble extending the landing gear on approach to GUM, indicated by a red light on the landing gear indicator and a warning horn. After aborting the initial approach and consulting a cockpit operations manual, the flight crew concluded the landing gear was "down and locked."

Soon after touchdown, the nose gear collapsed, and the plane skidded to a stop on the runway. The 340 persons aboard evacuated the stricken jet via inflatable slides, with only two minor injuries reported. The aircraft, damaged beyond all repair, was eventually scrapped, the Guam Pacific Daily News said.

Subsequent examination and testing of the aircraft's nose gear components revealed several problems with the landing gear door actuator: one of two "lock keys" was found to be installed backward; strands of metallic material were found in different areas of the actuator; the "manual override crank gland was found lightly torqued with safety wire installed"; the "lock ram and lock ring" were damaged; and the piston rod seal was "installed with non-standard backup rings," according to the report.

Unknown to the flight crew of Flight 74, the same aircraft had experienced similar problems just 10 days prior, but the captain of that flight failed to make note of it in the plane's maintenance log.

The NTSB's final report on the accident and determination of probable cause has not yet been released.

FMI: www.nwa.com, www.ntsb.org

Advertisement

More News

ANN's Daily Aero-Term (12.19.25): Ultrahigh Frequency (UHF)

Ultrahigh Frequency (UHF) The frequency band between 300 and 3,000 MHz. The bank of radio frequencies used for military air/ground voice communications. In some instances this may >[...]

NTSB Prelim: Cirrus Design Corp SR22T

During The 7 Second Descent, There Was Another TAWS Alert At Which Time The Engine Remained At Full Power On October 24, 2025 at 2115 mountain daylight time, a Cirrus SR22T, N740TS>[...]

Classic Aero-TV: The Red Tail Project--Carrying the Torch of the Tuskegee Airmen

From 2009 (YouTube Edition): Educational Organization Aims to Inspire by Sharing Tuskegee Story Founding leader Don Hinz summarized the Red Tail Project’s mission in simple, >[...]

Aero-News: Quote of the Day (12.19.25)

“This feels like an important step since space travel for people with disabilities is still in its very early days... I’m so thankful and hope it inspires a change in m>[...]

Airborne 12.17.25: Skydiver Hooks Tail, Cooper Rotax Mount, NTSB v NDAA

Also: New Katanas, Kern County FD Training, IndiGo’s Botched Roster, MGen. Leavitt Named ERAU Dean The Australian Transportation Safety Bureau (ATSB) has wrapped up its inves>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC