NTSB Prelim Report On Scottsdale Learjet Accident | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-12.01.25

AirborneNextGen-
12.02.25

Airborne-Unlimited-11.19.25

Airborne-AffordableFlyers-11.20.25

AirborneUnlimited-11.21.25

LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Mon, Mar 03, 2025

NTSB Prelim Report On Scottsdale Learjet Accident

Captain Fatally Injured, Four Others Injured

The NTSB released its preliminary report on the accident involving a Gates Learjet 35A on February 10, 2025, at Scottsdale Airport (SDL) in Arizona. The aircraft was substantially damaged while the captain was killed in the accident and four others were injured including an occupant of the parked aircraft that was struck by the accident aircraft.

The flight was operated as a Part 91 corporate flight to transport passengers to Arizona for a local event. The flight originated in Florida and made a refueling stop in Austin, Texas. At about 2:34 pm MST, at 2,800 ft AGL the aircraft turned onto an extended final approach for runway 21 at SDL.

Investigators were able to obtain security camera footage as well as videos recorded by witness cell phone cameras. A video provided by a witness taken from a golf course near the final approach captured the aircraft and it can be seen with its left main landing gear trailing aft from its normal position.

Immediately after the aircraft touched down on the runway it entered a left-wing low attitude and began veering left and exited the runway, traveling over the island between the runway and taxiways.

It crossed taxiway Bravo and entered the ramp area where it struck the right side of a parked Gulfstream G200. The aircraft was not equipped with thrust reversers and the drag chute was not deployed. The aircraft came to rest with its nose embedded between the right side of the Gulfstream’s fuselage and the inboard trailing edge of the right wing.

The engines of the accident airplane continued running until the fire truck arrived to spray foam on the right side engine to shut it down. One passenger was able to egress the aircraft but then went back to assist the other passenger. The captain sustained fatal injuries, the FO and one of the passengers were seriously injured, as was an occupant of the parked Gulfstream, and one passenger had minor injuries.

This is the NTSB’s preliminary report and the purpose is to convey the facts as currently known as the investigation continues. The final report will contain all the facts as subsequently discovered and ascribe a probable cause for the accident.

Relevant details include:

  • Location:         Scottsdale, Arizona
  • Date & Time:   February 10, 2025, 14.38 Local
  • Aircraft:            Gates Learjet Corp. 35A
  • Nature:            Part 91, General Aviation – Executive/Corporate
  • Accident #:      WPR25FA088
  • Registration:    N81VN
  • Injuries:           1 Fatal, 3 Serious, 1 Minor
FMI:  www.ntsb.gov/

Advertisement

More News

NTSB Prelim: Cirrus Design Corp SR20

The Airplane Made An Uncommanded Right Yaw And Roll, And He Was Unable To Maintain Control Of The Airplane On November 11, 2025, about 1750 central standard time, a Cirrus SR20, N8>[...]

ANN's Daily Aero-Linx (11.30.25)

Aero Linx: Florida Antique Biplane Association "Biplanes.....outrageous fun since 1903." That quote really defines what the Florida Antique Biplane Association (FABA) is all about.>[...]

ANN's Daily Aero-Term (11.30.25): Wind Shear Escape

Wind Shear Escape An unplanned abortive maneuver initiated by the pilot in command (PIC) as a result of onboard cockpit systems. Wind shear escapes are characterized by maximum thr>[...]

Aero-News: Quote of the Day (11.30.25)

“Working closely with the Polish Armed Forces, we’re focused on disciplined execution to help enhance Poland’s defense capabilities and keep up with the strong de>[...]

Airborne 11.26.25: Bonanza-Baron Fini, Archer v LA NIMBYs, Gogo Loses$$$

Also: Bell 505 on SAF, NYPA Gets Flak For BizAv 'Abuse', FAA Venezuela Caution, Horizon Update Textron Aviation has confirmed it will be ending production of the Beechcraft Bonanza>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC