NTSB Final Report: RANS S21 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-06.23.25

Airborne-NextGen-06.24.25

AirborneUnlimited-06.25.25

Airborne-AffordableFlyers-06.26.25

AirborneUnlimited-06.27.25

Mon, Apr 29, 2024

NTSB Final Report: RANS S21

Owner’s (Pilot) Failure To Properly Torque A Fuel Filter B-Nut Fitting, Which Likely Introduced Air Into The Fuel System

Location: Fairfield, Utah Accident Number: WPR22LA211
Date & Time: June 9, 2022, 10:45 Local Registration: N46JH
Aircraft: RANS S21 Aircraft Damage: Substantial
Defining Event: Fuel starvation Injuries: 1 Minor
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The pilot was conducting a test flight following recent maintenance when, shortly after departing, the engine began to lose power. He performed a forced landing on airport property, during which the airplane landed hard and sustained substantial damage.

Postaccident examination of the engine revealed that the fuel filter b-nut fitting was not properly torqued, which likely introduced air into the fuel system. Additionally, there was no restricted bypass line between the inlet (pressure side of the fuel pump module) and the return line and no vent line from the header tank, both of which would have allowed the venting of air from the fuel system. Based on this evidence, it is likely that the loose fuel filter b-nut allowed the air into the fuel system that could not be properly vented due to the lack of a restricted bypass line and vent line, which ultimately resulted in the loss of engine power.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The owner’s (pilot) failure to properly torque a fuel filter b-nut fitting, which likely introduced air into the fuel system and resulted in a loss of engine power. Contributing to the loss of power was a missing restricted bypass line and a header tank vent line, which would have allowed the venting of air from the fuel system.

FMI: www.ntsb.gov

Advertisement

More News

NTSB Final Report: Rutan Long-EZ

He Attempted To Restart The Engine Three Times. On The Third Restart Attempt, He Noticed That Flames Were Coming Out From The Right Wing Near The Fuel Cap Analysis: The pilot repor>[...]

ANN FAQ: Turn On Post Notifications

Make Sure You NEVER Miss A New Story From Aero-News Network Do you ever feel like you never see posts from a certain person or page on Facebook or Instagram? Here’s how you c>[...]

Classic Aero-TV: ICAS Perspectives - Advice for New Air Show Performers

From 2009 (YouTube Edition): Leading Air Show Performers Give Their Best Advice for Newcomers On December 6th through December 9th, the Paris Las Vegas Hotel hosted over 1,500 air >[...]

ANN's Daily Aero-Linx (06.28.25)

Aero Linx: NASA ASRS ASRS captures confidential reports, analyzes the resulting aviation safety data, and disseminates vital information to the aviation community. The ASRS is an i>[...]

Aero-News: Quote of the Day (06.28.25)

“For our inaugural Pylon Racing Seminar in Roswell, we were thrilled to certify 60 pilots across our six closed-course pylon race classes. Not only did this year’s PRS >[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC