NTSB Final Report: Zenith CH-750 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-11.24.25

AirborneNextGen-
11.18.25

Airborne-Unlimited-11.19.25

Airborne-AffordableFlyers-11.20.25

AirborneUnlimited-11.21.25

LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Tue, Aug 06, 2024

NTSB Final Report: Zenith CH-750

Flight Instructor Took Off, Turned Prematurely, And Clipped A Fence With The Right Wing

Location: Seymour, Indiana Accident Number: CEN24LA177
Date & Time: April 30, 2024, 15:00 Local Registration: N750EE
Aircraft: Zenith CH-750 Aircraft Damage: Substantial
Defining Event: Collision during takeoff/land Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Instructional

Analysis: The flight instructor reported that he was practicing short-field takeoffs and landings with the pilot-rated airplane owner. After multiple takeoffs and landings on the owner’s field, the flight instructor took off, turned prematurely, and clipped a fence with the right wing. The airplane flipped over, impacted terrain, and came to a rest inverted, which resulted in substantial damage to the forward fuselage and both wings. The flight instructor reported that there were no preimpact malfunctions or failures with the airplane that would have precluded normal operation.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The flight instructor’s failure to maintain clearance from a fence during a takeoff attempt.

FMI: www.ntsb.gov

Advertisement

More News

ANN's Daily Aero-Linx (11.25.25)

Aero Linx: Vintage Sailplane Association The purpose of the Vintage Sailplane Association (VSA) is to promote the acquisition, restoration and flying of vintage sailplanes by its m>[...]

NTSB Final Report: Glasair GlaStar

Smoke Began Entering The Cockpit During The Landing Flare, And Then The Pilot Noticed Flames... Analysis: The pilot reported that about 30 minutes into the local flight, he heard s>[...]

ANN FAQ: Turn On Post Notifications

Make Sure You NEVER Miss A New Story From Aero-News Network Do you ever feel like you never see posts from a certain person or page on Facebook or Instagram? Here’s how you c>[...]

Classic Aero-TV: Red Tail Project Update – Taking the Mission to the People

From 2010 (YouTube Edition): The Red Tail Project Continues Effort Towards ‘Rise Above Program’ The Red Tail Project is a true example of this unbreakable spirit. In 20>[...]

Airborne 11.24.25: ANN's 30th!, Starship’s V3 Booster Boom, Earhart Records

Also: 1st-Ever Space Crime Was a Fraud, IAE Buys Diamonds, Kennon Bows Out, Perseverance Rover An interesting moment came about this past Sunday as ANN CEO, Jim Campbell, noted tha>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC