NTSB Prelim: Cessna 182 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-06.23.25

Airborne-NextGen-06.24.25

AirborneUnlimited-06.25.25

Airborne-AffordableFlyers-06.26.25

AirborneUnlimited-06.27.25

Wed, Nov 18, 2020

NTSB Prelim: Cessna 182

Engine Initially Ran Smooth But Began Knocking And Vibrating

Location: Lebanon, OH Accident Number: CEN21LA034
Date & Time: October 28, 2020, 11:45 Local Registration: N3537C
Aircraft: Cessna 182 Injuries: 2 None
Flight Conducted Under:

On October 28, 2020, about 1145 eastern daylight time, a Cessna 182T airplane, N3537C, was substantially damaged when it was involved in an accident near Lebanon, Ohio. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot stated he and the passenger were ferrying the airplane from Clermont County Airport (I69), Ohio, to Warren County Airport (I68), Ohio following maintenance to install new avionics. While flying at 3,000 ft mean sea level (MSL) in instrument meteorological conditions the oil pressure dropped to zero. The engine initially ran smooth but began knocking and vibrating. The pilot declared an emergency and proceeded direct to I68, but was unable to maintain altitude. The airplane broke clear of the clouds about 600 ft above the ground and the engine subsequently lost all power. Unable to make the runway, the pilot elected to land in a harvested corn field. The pilot could not stop the airplane before it hit trees at the end of the field, damaging the airplane’s wings and fuselage.

The engine was examined, and a brightly colored plastic cap was found installed on the crankcase breather port, which completely blocked the port. The engine crankcase seal on the front of the engine was found dislodged and oil was found on the underside of engine compartment and cowling.

FMI: www.ntsb.gov

Advertisement

More News

NTSB Final Report: Rutan Long-EZ

He Attempted To Restart The Engine Three Times. On The Third Restart Attempt, He Noticed That Flames Were Coming Out From The Right Wing Near The Fuel Cap Analysis: The pilot repor>[...]

ANN FAQ: Turn On Post Notifications

Make Sure You NEVER Miss A New Story From Aero-News Network Do you ever feel like you never see posts from a certain person or page on Facebook or Instagram? Here’s how you c>[...]

Classic Aero-TV: ICAS Perspectives - Advice for New Air Show Performers

From 2009 (YouTube Edition): Leading Air Show Performers Give Their Best Advice for Newcomers On December 6th through December 9th, the Paris Las Vegas Hotel hosted over 1,500 air >[...]

ANN's Daily Aero-Linx (06.28.25)

Aero Linx: NASA ASRS ASRS captures confidential reports, analyzes the resulting aviation safety data, and disseminates vital information to the aviation community. The ASRS is an i>[...]

Aero-News: Quote of the Day (06.28.25)

“For our inaugural Pylon Racing Seminar in Roswell, we were thrilled to certify 60 pilots across our six closed-course pylon race classes. Not only did this year’s PRS >[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC