NTSB Finds Pilot Error In Maine Fatal Floatplane Accident | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-05.13.24

Airborne-NextGen-05.14.24

Airborne-Unlimited-05.15.24 Airborne-AffordableFlyers-05.16.24

Airborne-Unlimited-05.17.24

Fri, Oct 28, 2011

NTSB Finds Pilot Error In Maine Fatal Floatplane Accident

Pilot Failed to Retract The Landing Gear On The Amphib

The NTSB has released its probable cause report in a floatplane accident which occurred August 1st, 2010, in which a 64-year-old ATP rated pilot was fatally injured. A passenger on board the aircraft survived the accident.

According to the report, the amphibious float-equipped airplane departed from a paved runway for the flight, where a water landing on a lake was to be made. The pilot did not raise the landing gear after takeoff. Upon reaching the destination, the landing gear contacted the water during landing and the airplane abruptly nosed over. The airplane came to rest floating inverted, suspended by the floats. The month preceding the accident the pilot had several medical tests performed and was anticipating surgery for the removal of stomach cancer. While the pilot may have been having difficulty sleeping due to back pain or his impending surgery or possible chemotherapy, the investigation was unable to determine that fatigue was a factor in the accident. His toxicology results indicated recent use of diphenhydramine (an over-the-counter antihistamine) at levels that would have likely been impairing at the time of the accident.

According to a statement given by the passenger to an FAA inspector and the Maine State Police, just prior to the airplane making contact with the water, the pilot made a verbal expression and immediately after making contact with the water, the airplane went to the left and nosed over. She also informed the FAA inspector that they departed a paved surface at 8B0. The passenger reported to the Maine State Police that on the morning of the accident, the pilot "wasn't feeling well;" however, after breakfast "he was feeling much better and felt he was fine to fly." She also reported that "they had a normal flight" and the area of the accident was "the same area he always lands."

The NTSB determined the probable cause(s) of this accident to be the pilot's failure to retract the landing gear prior to a water landing. Contributing to the accident was the pilot's impairment due to medication.

FMI: www.ntsb.gov

Advertisement

More News

Bolen Gives Congress a Rare Thumbs-Up

Aviation Governance Secured...At Least For a While The National Business Aviation Association similarly applauded the passage of the FAA's recent reauthorization, contentedly recou>[...]

The SportPlane Resource Guide RETURNS!!!!

Emphasis On Growing The Future of Aviation Through Concentration on 'AFFORDABLE FLYERS' It's been a number of years since the Latest Edition of Jim Campbell's HUGE SportPlane Resou>[...]

Buying Sprees Continue: Textron eAviation Takes On Amazilia Aerospace

Amazilia Aerospace GmbH, Develops Digital Flight Control, Flight Guidance And Vehicle Management Systems Textron eAviation has acquired substantially all the assets of Amazilia Aer>[...]

Hawker 4000 Bizjets Gain Nav System, Data Link STC

Honeywell's Primus Brings New Tools and Niceties for Hawker Operators Hawker 4000 business jet operators have a new installation on the table, now that the FAA has granted an STC f>[...]

Echodyne Gets BVLOS Waiver for AiRanger Aircraft

Company Celebrates Niche-but-Important Advancement in Industry Standards Echodyne has announced full integration of its proprietary 'EchoFlight' radar into the e American Aerospace>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC