NTSB: NWA Flight 74 Crew Thought Gear Was Down | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-06.10.24

Airborne-NextGen-06.11.24

Airborne-Unlimited-06.12.24 Airborne-FltTraining-06.13.24

Airborne-Unlimited-06.14.24

Mon, Dec 22, 2008

NTSB: NWA Flight 74 Crew Thought Gear Was Down

Faulty Nose Gear Door Actuator Examined

The National Transportation Safety Board has released an updated factual report on the Northwest Airlines Flight 74 landing accident at Guam International Airport (GUM) on August 19, 2005.

As ANN reported, the NWA Boeing 747-200 experienced trouble extending the landing gear on approach to GUM, indicated by a red light on the landing gear indicator and a warning horn. After aborting the initial approach and consulting a cockpit operations manual, the flight crew concluded the landing gear was "down and locked."

Soon after touchdown, the nose gear collapsed, and the plane skidded to a stop on the runway. The 340 persons aboard evacuated the stricken jet via inflatable slides, with only two minor injuries reported. The aircraft, damaged beyond all repair, was eventually scrapped, the Guam Pacific Daily News said.

Subsequent examination and testing of the aircraft's nose gear components revealed several problems with the landing gear door actuator: one of two "lock keys" was found to be installed backward; strands of metallic material were found in different areas of the actuator; the "manual override crank gland was found lightly torqued with safety wire installed"; the "lock ram and lock ring" were damaged; and the piston rod seal was "installed with non-standard backup rings," according to the report.

Unknown to the flight crew of Flight 74, the same aircraft had experienced similar problems just 10 days prior, but the captain of that flight failed to make note of it in the plane's maintenance log.

The NTSB's final report on the accident and determination of probable cause has not yet been released.

FMI: www.nwa.com, www.ntsb.org

Advertisement

More News

ANN FAQ: Submit a News Story!

Have A Story That NEEDS To Be Featured On Aero-News? Here’s How To Submit A Story To Our Team Some of the greatest new stories ANN has ever covered have been submitted by our>[...]

Aero-News: Quote of the Day (06.12.24)

“The legislation now includes a task force with industry representation ensuring that we have a seat at the table and our voice will be heard as conversations about the futur>[...]

ANN's Daily Aero-Linx (06.12.24)

Aero Linx: Waco Museum The WACO Historical Society, in addition to preserving aviation's past, is also dedicated and actively works to nurture aviation's future through its Learnin>[...]

ANN's Daily Aero-Term (06.12.24): Adcock Range

Adcock Range National low-frequency radio navigation system (c.1930-c.1950) replaced by an omnirange (VOR) system. It consisted of four segmented quadrants broadcasting Morse Code >[...]

Airborne Affordable Flyers 06.06.24: 200th ALTO, Rotax SB, Risen 916iSV

Also: uAvionix AV-Link, Does Simming Make Better Pilots?, World Games, AMA National Fun Fly Czech sportplane manufacturer Direct Fly has finished delivering its 200th ALTO NG, the >[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC