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Mon, Feb 24, 2025

NTSB Final Report: Composite FX Mosquito XE

The Total Loss Of Engine Power And Subsequent Impact With Terrain During An Autorotation

Location: Waco, Texas Accident Number: CEN25LA038
Date & Time: November 11, 2024, 14:40 Local Registration: N869DJ
Aircraft: Composite FX Mosquito XE Aircraft Damage: Substantial
Defining Event: Loss of engine power (total) Injuries: 1 Minor
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The pilot stated that while returning to the airport, the helicopter’s engine rpm dropped to zero with no warning. He initiated an autorotation and aligned the helicopter to touch down in an open field but noticed powerlines as he got closer. The pilot maneuvered away from the field and aimed for a clearing in a residential backyard. The main rotor blades impacted a tree, and the helicopter fell about 15 ft to the ground before it came to rest on its right side. The helicopter sustained substantial damage to the fuselage and main rotor blades. According to maintenance records, the engine was removed and replaced about a month before the accident. Additionally, a condition inspection was completed by the owner four days before the accident during which he changed the spark plugs and adjusted the fuel mixture.

A post-accident examination revealed corrosion at the radiator fill tube connection and a loose band clamp. Additionally, the engine exhibited signatures consistent with being operated at a temperature above the normal operating temperatures and evidence of piston seizure due to thermal expansion.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The total loss of engine power and subsequent impact with terrain during an autorotation. Contributing to the accident was the improper sealing of the liquid cooling system.

FMI: www.ntsb.gov

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