NTSB Prelim: Beech A36 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-11.24.25

AirborneNextGen-
11.18.25

Airborne-Unlimited-11.19.25

Airborne-AffordableFlyers-11.20.25

AirborneUnlimited-11.21.25

LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Sat, Jun 05, 2021

NTSB Prelim: Beech A36

The Engine Began To Shake And Lost Total Power

Location: Pinckneyville, IL Accident Number: CEN21LA221
Date & Time: May 14, 2021, 15:00 Local Registration: N1875W
Aircraft: Beech A36 Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Personal

On May 14, 2021, at 1500 central daylight time, a Beech A36, N1875W, was substantially damaged when it was involved in an accident near Pinckneyville, Illinois. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, while at an altitude of 8,000 ft mean sea level, he noticed the engine oil pressure began to fluctuate. The pilot contacted air traffic control and requested to divert to the nearest airport, which was the Pinckneyville-Du Quoin Airport. Shortly thereafter, the engine began to shake and lost total power. Unable to make the airport, the pilot executed a forced landing to a field. During the forced landing, the airplane’s nose wheel landing gear impacted a ditch. The nose landing gear collapsed, and the airplane came to rest upright.

The airplane sustained substantial damage to the left wing and fuselage. Visual examination of the engine revealed a hole in the engine crankcase.

FMI: www.ntsb.gov

Advertisement

More News

ANN's Daily Aero-Linx (11.25.25)

Aero Linx: Vintage Sailplane Association The purpose of the Vintage Sailplane Association (VSA) is to promote the acquisition, restoration and flying of vintage sailplanes by its m>[...]

NTSB Final Report: Glasair GlaStar

Smoke Began Entering The Cockpit During The Landing Flare, And Then The Pilot Noticed Flames... Analysis: The pilot reported that about 30 minutes into the local flight, he heard s>[...]

ANN FAQ: Turn On Post Notifications

Make Sure You NEVER Miss A New Story From Aero-News Network Do you ever feel like you never see posts from a certain person or page on Facebook or Instagram? Here’s how you c>[...]

Classic Aero-TV: Red Tail Project Update – Taking the Mission to the People

From 2010 (YouTube Edition): The Red Tail Project Continues Effort Towards ‘Rise Above Program’ The Red Tail Project is a true example of this unbreakable spirit. In 20>[...]

Airborne 11.24.25: ANN's 30th!, Starship’s V3 Booster Boom, Earhart Records

Also: 1st-Ever Space Crime Was a Fraud, IAE Buys Diamonds, Kennon Bows Out, Perseverance Rover An interesting moment came about this past Sunday as ANN CEO, Jim Campbell, noted tha>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC