Newsday Says Close Pass Due to Staffing Levels | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-SpecialEpisode-12.15.25

AirborneNextGen-
12.16.25

Airborne-Unlimited-12.10.25

Airborne-AffordableFlyers-12.11.25

AirborneUnlimited-12.12.25

AFE 2025 LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Wed, May 07, 2003

Newsday Says Close Pass Due to Staffing Levels

Highlights Chronic Problem, Article Says

Sylvia Adcock, who writes for Newsday.com, has filed a story that might scare a lot of folks. She says that a Delta 767 and a Sunjet MD-80 nearly merged in the sky on April 27, and that the union told her that "...the controller was distracted by other duties and that the mistake was human error that stemmed from inadequate staffing levels."

The FAA says the union may be grandstanding, using a controller screw-up to wrest more money out of the system. The union was reported as having said that the controller, working alone at the New York Air Route Traffic Control Center in Ronkonkoma, just ran out of buffer space in the ol' noggin, and had a momentary lapse of concentration, that let the MD-80 slip through. That lapse, the case is being made, was due to work rules and pay.

The radar system in the center alerted the controller, who instructed the Delta flight to make appropriate corrections. Neither pilot filed a report; the planes passed more than 500 feet from each other, technically disqualifying the incident as a "near miss." (At 600 feet and a mile-plus, it didn't qualify; but it was close enough to make the union's point.)

Adcock noted, "The FAA said staffing was not an issue in the mistake. Rick Ducharme, manager of air traffic for the FAA's eastern region, said the controller was handling only six planes, a relatively light load. He said the controller didn't ask for help, and with several controllers on break, one could have been pulled in to help." In fact, traffic was about to double, and another controller was on the way, when the slip-up occured.

FMI: www.faa.gov; www.natca.org

Advertisement

More News

Aero-News: Quote of the Day (12.18.25)

“These new aircraft strengthen our ability to respond quickly, train effectively and support communities nationwide. Textron Aviation has been a steadfast supporter in helpin>[...]

Classic Aero-TV: Viking Twin Otter 400--Bringing the DHC-6 Back Into Production

From 2011 (YouTube Edition): Rugged, Legendary, STOL Twin Makes A Comeback The de Havilland Twin Otter is an airplane with a long history, and it gained a reputation as a workhorse>[...]

NTSB Final Report: Rans Employee Flying Club Rans S-6ES Coyote II

A Wind Gust Lifted The Right Wing And The Airplane Turned To The Left Analysis: The pilot was departing from a 2,395-ft-long by 50-ft-wide turf runway. The pilot reported that afte>[...]

ANN FAQ: Submit a News Story!

Have A Story That NEEDS To Be Featured On Aero-News? Here’s How To Submit A Story To Our Team Some of the greatest new stories ANN has ever covered have been submitted by our>[...]

ANN's Daily Aero-Term (12.18.25): Braking Action Advisories

Braking Action Advisories When tower controllers receive runway braking action reports which include the terms “medium," “poor," or “nil," or whenever weather con>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC