NTSB Final Report: Progressive Aerodyne Inc Searey LSA | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-12.08.25

AirborneNextGen-
12.09.25

Airborne-Unlimited-12.10.25

Airborne-AffordableFlyers-12.11.25

AirborneUnlimited-12.12.25

AFE 2025 LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Thu, Apr 25, 2024

NTSB Final Report: Progressive Aerodyne Inc Searey LSA

Information Indicates The Flight Crew Failed To Assure There Was An Adequate Fuel Supply

Location: Detroit, Michigan Accident Number: CEN23LA214
Date & Time: May 31, 2023, 20:30 Local Registration: N316SR
Aircraft: Progressive Aerodyne Inc Searey LSA Aircraft Damage: Substantial
Defining Event: Fuel exhaustion Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The airplane was returning to the departure airport after a local training flight when the engine lost all power. Restart attempts were not successful. The pilot reported that he glanced at the fuel gauge and it indicated ¼ full. During the forced landing the airplane contacted trees, which resulted in substantial damage to the left wing.

Examination of the airplane after the accident revealed that only a trace amount of fuel was visible in the semi-transparent plastic fuel tank; the tank did not appear to be breached. After the airplane was removed from the accident site and leveled on a trailer used for recovery, the fuel gauge read empty. A subsequent engine run was performed where fuel was added to the tank and the engine started. The engine was operated from idle to full throttle and no anomalies were detected during the engine run.

Based on the pilot’s report, the flight duration was about 2.5 hours; however, recorded flight track data indicated the flight actually lasted 3 hours. Available information indicates the flight crew failed to assure there was an adequate fuel supply for the flight, which resulted in fuel exhaustion and a complete loss of engine power. 

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- A loss of engine power due to fuel exhaustion that resulted from the pilots’ inadequate preflight planning.


FMI: www.ntsb.gov 

Advertisement

More News

ANN FAQ: Contributing To Aero-TV

How To Get A Story On Aero-TV News/Feature Programming How do I submit a story idea or lead to Aero-TV? If you would like to submit a story idea or lead, please contact Jim Campbel>[...]

Aero-News: Quote of the Day (12.10.25)

“As the excitement builds for the world of flight returning to Oshkosh in 2026, we wanted to ensure that advance tickets are available for those who enjoy giving AirVenture t>[...]

ANN's Daily Aero-Term (12.10.25): North Atlantic High Level Airspace (NAT HLA)

North Atlantic High Level Airspace (NAT HLA) That volume of airspace (as defined in ICAO Document 7030) between FL 285 and FL 420 within the Oceanic Control Areas of Bodo Oceanic, >[...]

Airborne 12.08.25: Samaritan’s Purse Hijack, FAA Med Relief, China Rocket Fail

Also: Cosmonaut Kicked Out, Airbus Scales Back, AF Silver Star, Russian A-60 Clobbered A Samaritan’s Purse humanitarian flight was hijacked on Tuesday, December 2, while atte>[...]

Airborne-Flight Training 12.04.25: Ldg Fee Danger, Av Mental Health, PC-7 MKX

Also: IAE Acquires Diamond Trainers, Army Drones, FedEx Pilots Warning, DA62 MPP To Dresden Tech Uni The danger to the flight training industry and our future pilots is clear. Dona>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC