Says O2 System Functioned Normally When Checked
Editor's Note: The National Transportation
Safety Board has released its preliminary report on a February 2
incident involving a Beechcraft B200 King Air that suffered a
cracked windscreen at FL270.
As Aero-News
reported, the plane's pilots depressurized
the cockpit and put on their oxygen masks, but were unable to begin
the flow of oxygen before passing out. Fortunately, the pilots
regained consciousness as the aircraft descended, and they were
able to land the plane, as the Board notes dryly, "without further
incident."
In the report -- which is presented, unedited, below
-- the NTSB notes the aircraft's oxygen system operated
normally when investigators engaged its controls as defined by the
plane's flight manual.
NTSB Identification:
CHI07LA063
14 CFR Part 91: General Aviation
Accident occurred Friday, February 02, 2007 in Cape Girardeau,
MO
Aircraft: Raytheon Aircraft Company B200, registration:
N777AJ
Injuries: 2 Uninjured.
This is preliminary information, subject to change, and may
contain errors. Any errors in this report will be corrected when
the final report has been completed.
On February 2, 2007, about 1030 central standard time, a
Raytheon Aircraft Company B200, N777AJ, sustained substantial
damage during an uncontrolled descent and recovery from cruise at
flight level 270. Visual meteorological conditions prevailed at the
time of the accident.
The flightcrew reported that they depressurized the airplane
after noticing cracking of the airplane windshield. They then
donned their oxygen masks but were unable to obtain oxygen from the
oxygen system resulting in their loss of consciousness. They later
regained consciousness, recovered from the descent, and landed
without further incident at Cape Girardeau Regional Airport, Cape
Girardeau, Missouri.
The 14 CFR Part 91 flight was operating on an instrument rules
flight plan. The pilot and copilot were uninjured. The flight
originated from Rogers Municipal Airport-Carter Field, Rogers,
Arkansas, at 0939.
On-scene inspection of the airplane noted that approximately 2/3
of the left horizontal stabilizer and elevator were separated from
the aircraft and 2/3 of the right elevator was separated but
attached at the inboard hinge. The left and right wings were
wrinkled. The left pilot windshield outer and inner ply were
intact. The inner ply exhibited a shattered appearance with a crack
at the lower right hand corner of the windshield. The cabin
pressurization dump switch was in the dump position.
The oxygen system worked when it was functionally tested in
accordance with Airplane Flight Manual.
(Screen captures of video footage shown on KFVS-12)