NTSB Releases Probable Cause Report On 2006 Baron Accident | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.22.24

Airborne-Unlimited-04.16.24

Airborne-FlightTraining-04.17.24 Airborne-AffordableFlyers-04.18.24

Airborne-Unlimited-04.19.24

Join Us At 0900ET, Friday, 4/10, for the LIVE Morning Brief.
Watch It LIVE at
www.airborne-live.net

Tue, Jun 19, 2007

NTSB Releases Probable Cause Report On 2006 Baron Accident

States Pilot Error, Oxygen Deprivation Led To Fatal Crash

The National Transportation Safety Board ruled this week the pilot's failure to ensure an adequate supply of supplemental oxygen led to the March 17, 2006 downing of a Beechcraft Baron 56TC in West Virginia.

As ANN reported, William Cammack was enroute from Glendive, MT to Minnesota's St. Paul Downtown Airport when air traffic controllers lost contact with the pilot, as his plane continued to fly on course at FL270.

The Wisconsin National Guard deployed two F-16s to intercept the aircraft after it flew over the Twin Cities area, and turned southeast. Two other F-16s met the aircraft as it crossed into Michigan. Those fighters flanked the Baron throughout the remainder of its flight, and attempted to contact the pilot several times with no success.

After about two hours, the F-16 pilots could only watch helplessly as the Baron evidently ran out of fuel, and went down in a clearing near Winfield, WV. The crash missed a nearby house by about 250 feet.

The NTSB states Cammack's logbooks indicated he preferred to fly in the flight levels for engine efficiency. His aircraft was equipped with an onboard supplemental oxygen system, connected to a nasal cannula that was found near the pilot's body. Cammack was wearing an oxygen mask, connected to a non-aviation-grade portable oxygen tank.

Investigators found both systems intact, but empty. There were no records of either system being serviced throughout Cammack's multi-day trip.

"The pilot's inadequate preflight preparation to ensure adequate supply of supplemental oxygen, and his inadequate in-flight planning and decision making, which resulted in exhaustion of his oxygen supply, and incapacitation from hypoxia during cruise flight" likely caused the crash, the NTSB said in its report.

FMI: Read The Complete NTSB Probable Cause Report

Advertisement

More News

ANN's Daily Aero-Term (04.25.24): Airport Rotating Beacon

Airport Rotating Beacon A visual NAVAID operated at many airports. At civil airports, alternating white and green flashes indicate the location of the airport. At military airports>[...]

ANN's Daily Aero-Linx (04.25.24)

Aero Linx: Fly for the Culture Fly For the Culture, Inc. is a 501(c)(3) non-profit organization that serves young people interested in pursuing professions in the aviation industry>[...]

Klyde Morris (04.22.24)

Klyde Is Having Some Issues Comprehending The Fed's Priorities FMI: www.klydemorris.com>[...]

Airborne 04.24.24: INTEGRAL E, Elixir USA, M700 RVSM

Also: Viasat-uAvionix, UL94 Fuel Investigation, AF Materiel Command, NTSB Safety Alert Norges Luftsportforbund chose Aura Aero's little 2-seater in electric trim for their next gli>[...]

Airborne 04.22.24: Rotor X Worsens, Airport Fees 4 FNB?, USMC Drone Pilot

Also: EP Systems' Battery, Boeing SAF, Repeat TBM 960 Order, Japan Coast Guard H225 Buy Despite nearly 100 complaints totaling millions of dollars of potential fraud, combined with>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC