NTSB Final Report: Cessna 172C | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-12.08.25

AirborneNextGen-
12.02.25

Airborne-Unlimited-12.03.25

Airborne-FltTraining-12.04.25

AirborneUnlimited-12.05.25

AFE 2025 LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Thu, Apr 18, 2024

NTSB Final Report: Cessna 172C

After Flying For About 4 Hours, The Engine Lost Power And (Pilot) Executed A Forced Landing On A Road

Location: Wichita, Kansas Accident Number: CEN24LA019
Date & Time: October 20, 2023, 18:55 Local Registration: N1413Y
Aircraft: Cessna 172C Aircraft Damage: Substantial
Defining Event: Fuel exhaustion Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The pilot reported that she filled the airplane with fuel before departure. After flying for about 4 hours, the engine lost power and she executed a forced landing on a road about 1.5 miles from the destination airport. During the landing roll, the airplane impacted two street signs and a power pole guy wire which resulted in substantial damage to the airplane’s left wing and fuselage. The pilot reported that there were no preaccident mechanical malfunctions or failures that would have precluded normal operation.

Postaccident examination of the airplane revealed no anomalies with the fuel system; the fuel tanks were empty, and there was no evidence of a fuel leak. About 8 ounces of fuel were recovered from the gascolator. 

The pilot noted that verification of total fuel onboard before each departure and more accurate usage of the airplane’s performance charts could have prevented the accident.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s inadequate preflight inspection and fuel planning and improper in-flight decisionmaking, which resulted in a total loss of engine power due to fuel exhaustion. 

FMI: www.ntsb.gov

Advertisement

More News

NTSB Final Report: Patriot Aircraft LLC CX1900A

After Draining Both Wing Fuel Tanks, A Significant Amount Of Water Was Observed In The Right Wing Fuel Tank Analysis: The pilot, who was also the owner of the experimental amateur->[...]

Aero-News: Quote of the Day (12.06.25)

“Airbus apologises for any challenges and delays caused to passengers and airlines by this event. The Company thanks its customers, the authorities, its employees and all rel>[...]

ANN's Daily Aero-Term (12.06.25): High Speed Taxiway

High Speed Taxiway A long radius taxiway designed and provided with lighting or marking to define the path of aircraft, traveling at high speed (up to 60 knots), from the runway ce>[...]

ANN's Daily Aero-Linx (12.06.25)

Aero Linx: Taylorcraft Foundation, Inc. The Taylorcraft Foundation is exclusively organized for charitable, educational & scientific activities and will preserve the history an>[...]

Airborne-NextGen 12.02.25: Honda eVTOL, Arctus High-Alt UAS, Samson Patent

Also: USAF Reaper Accident, Baikonur Damage, Horizon eVTOL IFR/FIKI, New Glenn Update Honda has outlined its clearest timeline yet for its entry into the world of electric vertical>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC