NTSB Final Report: BC12-65 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-06.23.25

Airborne-NextGen-06.24.25

AirborneUnlimited-06.25.25

Airborne-AffordableFlyers-06.26.25

AirborneUnlimited-06.27.25

Fri, Aug 02, 2024

NTSB Final Report: BC12-65

About 25-30 Ft Above The Ground During The Initial Climb The Engine Suddenly Lost About 1,000 RPM

Location: Columbia, Tennessee  Date & Time: November 11, 2023, 08:15 Local 
Aircraft:Taylorcraft BC12-65  Defining Event: Fuel related
Flight Conducted Under: Part 91: General aviation - Personal
Accident Number: ERA24LA032  Registration: N29868
Aircraft Damage: Substantial  Injuries: 1 Minor

Analysis: The pilot was preparing for takeoff after the engine had been running for about 25 minutes. Before departing, he tested the carburetor heat and noted that it was functioning as expected. 

He applied power for takeoff and the engine accelerated “strongly and smoothly.” About 25-30 ft above the ground during the initial climb the engine suddenly lost about 1,000 rpm. The pilot elected to perform an off-field landing. He maneuvered to avoid a hedgerow and the airplane 
touched down in an in an area of high grass. During the landing sequence, the fuselage and right wing were substantially damaged. 

A postaccident examination of the engine and fuel system did not reveal evidence of a preexisting anomaly or failure that would have precluded normal operation. The temperature/dew point at the time of the accident was in the range for serious carburetor icing at cruise power. While the pilot described checking the functionality of the carburetor heat before as part of his normal preflight checks, and leaving it on for “a little longer” than normal as a part of that process, given all available information, it is likely that the temperature of the carburetor dropped during the extended operation of the engine while on the ground, and that during takeoff, the carburetor accumulated ice to a point that resulted in the partial loss of engine power.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- A partial loss of engine power due to an accumulation of carburetor ice, resulting in an off airport landing and substantial damage to the airplane.

FMI: www.ntsb.gov

Advertisement

More News

Airborne 06.30.25: US v ADS-B Misuse, Nat’l STOL Fire, Volocopter Resumes

Also: Netherlands Donates 18 F16s, 2 737s Collide On Ramp, E-7 Wedgetail Cut, AgEagle's 100th In S Korea The Pilot and Aircraft Privacy Act was introduced in the House by Represent>[...]

NTSB Prelim: Piper PA-23

Pilot Also Reported That Due To A Fuel Leak, The Auxiliary Fuel Tanks Were Not Used On June 4, 2025, at 13:41 eastern daylight time, a Piper PA-23, N2109P, was substantially damage>[...]

ANN FAQ: Submit a News Story!

Have A Story That NEEDS To Be Featured On Aero-News? Here’s How To Submit A Story To Our Team Some of the greatest new stories ANN has ever covered have been submitted by our>[...]

Classic Aero-TV: One Man’s Vietnam

From 2023 (YouTube Edition): Reflections on War’s Collective Lessons and Cyclical Nature The exigencies of war ought be colorblind. Inane social-constructs the likes of racis>[...]

Klyde Morris (06.30.25)

What Goes Around, May Yet Come Back Around, Klyde FMI: www.klydemorris.com>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC