NTSB Final Report: Allyn Kaste Rans S-19 (KIT) | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-SpecialEpisode-12.15.25

AirborneNextGen-
12.16.25

Airborne-Unlimited-12.10.25

Airborne-AffordableFlyers-12.11.25

AirborneUnlimited-12.12.25

AFE 2025 LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Sat, May 17, 2025

NTSB Final Report: Allyn Kaste Rans S-19 (KIT)

Engine Output Immediately Reduced To Idle Power And The Engine Would Not Respond To Throttle Input

Location: Doylestown, Pennsylvania Accident Number: ERA25LA122
Date & Time: February 10, 2025, 11:01 Local Registration: N258DK
Aircraft: Allyn Kaste Rans S-19 (KIT) Aircraft Damage: Substantial
Defining Event: Loss of engine power (partial) Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The day before the accident, the pilot had removed the airplane’s induction air filter but had inadvertently forgotten to reinstall it. On the day of the accident flight, he had also inadvertently forgotten to remove the engine cowling plugs. After takeoff, the pilot turned onto the downwind leg of the airport traffic pattern and the engine output immediately reduced to idle power and the engine would not respond to throttle input. The pilot then executed a forced landing in a gravel lot, during which the airplane bounced, the nose landing gear separated, and the airplane came to rest inverted. The airplane sustained substantial damage to the right wing and fuselage.

Postaccident examination of the wreckage confirmed that the left cowling plug was partially ingested into the end of the intake filter duct, completely obstructing it. No evidence of any preimpact mechanical malfunctions or failures of the airframe or engine were otherwise found. Based on this information, it is likely that the restricted flow of intake air to the engine resulted in the partial loss of engine power.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s inadequate maintenance and preflight inspection. 

FMI: www.ntsb.gov

Advertisement

More News

ANN's Daily Aero-Term (12.14.25): Local Airport Advisory (LAA)

Local Airport Advisory (LAA) A service available only in Alaska and provided by facilities that are located on the landing airport, have a discrete ground-to-air communication freq>[...]

Airborne 12.08.25: Samaritan’s Purse Hijack, FAA Med Relief, China Rocket Fail

Also: Cosmonaut Kicked Out, Airbus Scales Back, AF Silver Star, Russian A-60 Clobbered A Samaritan’s Purse humanitarian flight was hijacked on Tuesday, December 2, while atte>[...]

ANN's Daily Aero-Linx (12.15.25)

Aero Linx: Michigan Helicopter Association (MHA) The Michigan Helicopter Association (MHA) exists to bring together people who share an interest in helicopters, including private, >[...]

Airborne 12.10.25: New Gulfstream, ATC Integrator, Outrageous FFZ User Fees

Also: Airbus Acquisition, USCG Helo Sniper, Remember Pearl Harbor, New Thunderbird 1 Gulfstream’s newest addition to its next-gen lineup, the super-midsize G300, is officiall>[...]

Airborne-NextGen 12.09.25: Amazon Crash, China Rocket Accident, UAV Black Hawk

Also: Electra Goes Military, Miami Air Taxi, Hypersonics Lab, MagniX HeliStrom Amazon’s Prime Air drones are back in the spotlight after one of its newest MK30 delivery drone>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC