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NTSB Final Report: Kjelsrud Gary Kitfox

Airplane Exhibited A Partial Loss Of Engine Power When It Was About Halfway Down The Runway

Location: Powell, Wyoming Accident Number: WPR24LA148
Date & Time: May 10, 2024, 10:30 Local Registration: N605GK
Aircraft: Kjelsrud Gary Kitfox Aircraft Damage: Substantial
Defining Event: Loss of engine power (partial) Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The pilot of the experimental amateur-built airplane was departing from his private dirt strip when the accident occurred. The airplane exhibited a partial loss of engine power when it was about halfway down the runway. The pilot elected to proceed with the takeoff due to an irrigation canal at the end of the runway. The airplane would not gain altitude and subsequently struck two fences before nosing over and coming to rest inverted in a nearby yard.

Postaccident examination of the engine revealed that one of the two piston-type carburetors had the retaining clip for the jet needle set to the leanest position. The other carburetor was set to the engine manufacturer’s specified position. It is likely that the overly lean setting in one of the carburetors caused the carburetors not to be synchronized, which resulted in the partial loss of engine power during takeoff. According to the pilot, he adjusted the carburetor’s retaining clip to lower the cylinder temperature while he was flying in a different state and did not notice any loss of engine performance. However, this was his first attempted takeoff in Wyoming, that was located at a high elevation.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s adjustment of the carburetor to an incorrect setting, which resulted in partial loss of engine power during takeoff. 

FMI: www.ntsb.gov

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