NTSB Final Report: Hagerty Glasair Super IIS-TD | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-11.17.25

AirborneNextGen-
11.11.25

Airborne-Unlimited-11.12.25

Airborne-FltTraining-11.13.25

AirborneUnlimited-11.14.25

LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Mon, Apr 22, 2024

NTSB Final Report: Hagerty Glasair Super IIS-TD

During The Climb, About 4,500 Ft Mean Sea Level, The Engine Began To Run Rough, And Shortly Thereafter Lost All Power

Location: Jasper, Georgia Accident Number: ERA23LA063
Date & Time: November 4, 2022, 15:00 Local Registration: N430JV
Aircraft: Hagerty Glasair Super IIS-TD Aircraft Damage: Substantial
Defining Event: Sys/Comp malf/fail (non-power) Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis: The pilot reported that during the climb, about 4,500 ft mean sea level, the engine began to run rough, and shortly thereafter lost all power. The pilot immediately turned back toward the departure airport, which was about 5 miles from his position. He began troubleshooting the loss of power, but power was not restored. The pilot was able to glide to the airport; however, in a right turn to align with the runway, the pilot felt the onset of an aerodynamic stall. He leveled the wings, the airplane overshot the runway, descended abruptly, and impacted a grass area hard next to the runway. The left wing and fuselage sustained substantial damage. 

A postaccident test run of the engine revealed it produced normal power with the electric fuel pump on, but would not operate with only the engine-driven fuel pump. Further examination and disassembly of the engine-driven fuel pump revealed no anomalies that would have explained its inability to pump fuel.

The pilot reported that in the climb he turned off the electric fuel pump and, after the loss of power, he did not turn the pump back on, despite the owner’s manual instructing pilots to use the electric fuel pump following a loss of engine power. Had the pilot turned the electric fuel pump on, power likely would have been restored.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The loss of engine power due to the failure of the engine-driven fuel pump and the pilot’s failure to use the electric fuel pump, which resulted in a forced, hard landing. 

FMI: www.ntsb.gov

Advertisement

More News

Aero-News: Quote of the Day (11.17.25)

“We achieved full mission success today, and I am so proud of the team. It turns out Never Tell Me The Odds had perfect odds—never before in history has a booster this >[...]

ANN's Daily Aero-Term (11.17.25): NonDirectional Beacon

NonDirectional Beacon An L/MF or UHF radio beacon transmitting nondirectional signals whereby the pilot of an aircraft equipped with direction finding equipment can determine his/h>[...]

NTSB Final Report: Fred L Wellman CH 750 Cruzer

About 5ft Above Ground Level, The Airplane Stalled, And The Left Wing Dropped Analysis: The pilot reported that this flight was conducted as part of phase 1 flight testing of the n>[...]

ANN's Daily Aero-Linx (11.17.25)

Aero Linx: Brodhead Pietenpol Association The Brodhead Pietenpol Association is a newly reorganized (in 2017) non-profit educational corporation that grew and developed from an ear>[...]

Airborne-NextGen 11.11.25: Archer Buys Hawthorne, Joby Conforms, Stranded Astros

Also: VerdeGo Contract, Medi-Carrier, Gambit 6 UCAV, Blade Urban Air Mobility Pilot Archer Aviation has inked a deal for control of Hawthorne Municipal Airport (HHR), also known as>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC