NTSB Final Report: Piper PA-22-160 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-10.06.25

AirborneNextGen-
10.07.25

Airborne-Unlimited-10.08.25

Airborne-FlightTraining-10.09.25

AirborneUnlimited-10.10.25

Sat, Oct 07, 2023

NTSB Final Report: Piper PA-22-160

Shortly After Takeoff, The Engine Lost Power And The Propellor Began To Windmill

Location: Kenai, Alaska Accident Number: ANC23LA005
Date & Time: October 26, 2022, 16:56 Local Registration: N8119D
Aircraft: Piper PA-22-160 Aircraft Damage: Substantial
Defining Event: Loss of engine power (total) Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Instructional

Analysis: Shortly after takeoff, the engine lost power and the propellor began to windmill. The flight instructor conducted emergency procedures but was unable to regain engine power. The flight instructor determined that they did not have sufficient altitude to make it back to the airport and he selected a road on which to make a forced landing. To avoid a car, the pilot turned slightly towards the edge of the road and was pulled into a snow berm, where the aircraft came to a full stop. The airplane sustained substantial damage to the right wing and fuselage. 

A postaccident examination of the engine found the crankshaft drive gear bolt was missing and the gear alignment dowel pin on the crankshaft was broken. The missing bolt was not found during the postaccident examination. The engine was last disassembled in 1983 and the accessory gearbox was opened for an oil pump rebuild in 2006; the investigation was not able to identify how long the engine had operated with the bolt missing. The crankshaft drive gear drives the accessory gear box and, according to the engine manufacturer, failure of the gear or the gear attaching parts would result in complete engine stoppage. 

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- Improper installation of the crankshaft drive gear by maintenance personnel, who failed to install all required hardware, resulting in an in-flight engine failure.

FMI: www.ntsb.gov

Advertisement

More News

Airborne 10.14.25: Laser Threat, VeriJet BK, Duffy Threatens Problem Controllers

Also: USAF Pilots, Atlanta Tower Evac, Archer Spotlight Dissipates, Hop-A-Jet Sues A social-media call for people to point lasers at aircraft flying over Portland’s ICE facil>[...]

Airborne 10.15.25: Phantom 3500 Confounds, Citation CJ3 Gen2 TC, True Blue Power

Also: Kodiak 100 Joins USFS, Innovative Solutions & Support Renamed, Gulfstream Selects Honeywell, Special Olympics Airlift The Phantom 3500 mockup made an appearance where the>[...]

Aero-News: Quote of the Day (10.17.25)

"On the way back to the United States from NATO’s Defense Ministers meeting, Secretary of War Hegseth’s plane made an unscheduled landing in the United Kingdom due to a>[...]

NTSB Prelim: Piper PA-28-180

Pilot Was Transporting His Family Back To Their Home In Boise And He Planned To Fly Back To SHR That Afternoon On September 1, 2025 about 1612 mountain daylight time, a Piper PA-28>[...]

ANN FAQ: Contributing To Aero-TV

How To Get A Story On Aero-TV News/Feature Programming How do I submit a story idea or lead to Aero-TV? If you would like to submit a story idea or lead, please contact Jim Campbel>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC