NTSB Prelim: Cirrus Design Corp SR22 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-12.01.25

AirborneNextGen-
12.02.25

Airborne-Unlimited-11.19.25

Airborne-AffordableFlyers-11.20.25

AirborneUnlimited-11.21.25

LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Wed, Nov 06, 2024

NTSB Prelim: Cirrus Design Corp SR22

(Pilot) Identified A Potential Landing Area And Pulled The Cirrus Airframe Parachute System, But The Parachute Did Not Deploy

Location: Bakersfield, CA Accident Number: WPR25LA001
Date & Time: October 2, 2024, 13:47 Local Registration: N752B
Aircraft: Cirrus Design Corp SR22 Injuries: 1 Serious
Flight Conducted Under: Part 91: General aviation - Personal

On October 2, 2024, about 1347 Pacific daylight time, a Cirrus SR22, N752B, was substantially damaged when it was involved in an accident near Bakersfield, California. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, he refueled the airplane and departed Tulare, California, with about 75 gallons of 100 low lead aviation grade gasoline onboard and the low boost pump on. After departure, he climbed to 13,000 ft mean sea level (msl). When the pilot turned the low boost pump off the engine immediately started to run rough and began misfiring. The pilot then declared an emergency and the engine started to lose power. He attempted to run the engine on the high boost pump, which reduced the engine roughness; however, he was unsuccessful in restoring engine power.

At 1,200 ft msl, he identified a potential landing area and pulled the Cirrus Airframe Parachute System, but the parachute did not deploy. After the pilot pulled the cable a second time the parachute deployed, and the airplane leveled out. The pilot did not recall any further details from his recount of the accident.

Surveillance video captured the airplane’s final 4 seconds of flight, which showed the airplane’s shadow as it traversed a road. The airplane and its parachute came into view in the remaining two seconds of video, which showed it impact the ground in a nose low and right wing low attitude. The parachute then settled near the main wreckage.

Postaccident examination of the airplane revealed that fuselage and right wing was substantially damaged. The airplane has been retained for further examination. 

FMI: www.ntsb.gov

Advertisement

More News

NTSB Prelim: Cirrus Design Corp SR20

The Airplane Made An Uncommanded Right Yaw And Roll, And He Was Unable To Maintain Control Of The Airplane On November 11, 2025, about 1750 central standard time, a Cirrus SR20, N8>[...]

ANN's Daily Aero-Linx (11.30.25)

Aero Linx: Florida Antique Biplane Association "Biplanes.....outrageous fun since 1903." That quote really defines what the Florida Antique Biplane Association (FABA) is all about.>[...]

ANN's Daily Aero-Term (11.30.25): Wind Shear Escape

Wind Shear Escape An unplanned abortive maneuver initiated by the pilot in command (PIC) as a result of onboard cockpit systems. Wind shear escapes are characterized by maximum thr>[...]

Aero-News: Quote of the Day (11.30.25)

“Working closely with the Polish Armed Forces, we’re focused on disciplined execution to help enhance Poland’s defense capabilities and keep up with the strong de>[...]

Airborne 11.26.25: Bonanza-Baron Fini, Archer v LA NIMBYs, Gogo Loses$$$

Also: Bell 505 on SAF, NYPA Gets Flak For BizAv 'Abuse', FAA Venezuela Caution, Horizon Update Textron Aviation has confirmed it will be ending production of the Beechcraft Bonanza>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC