Sat, Dec 12, 2020
AD 2020-25-12 Prompted By Three Crankshaft Assembly Failures That Resulted In The Loss Of Engine Power
The FAA is adopting a new airworthiness directive (AD) for all Superior Air Parts, Inc. (SAP) Model IO-360-series and O-360-series reciprocating engines and certain Lycoming Engines (Lycoming) Model AEIO-360-, IO-360-, and O-360-series reciprocating engines with a certain SAP crankshaft assembly installed.

This SAP crankshaft assembly is installed as original equipment on the affected SAP engines and as a replacement part under parts manufacturer approval (PMA) on the affected Lycoming engines. This AD was prompted by three crankshaft assembly failures that resulted in the loss of engine power and immediate or emergency landings. This AD requires the removal from service of all affected crankshaft assemblies. The FAA is issuing this AD to address the unsafe condition on these products. This AD is effective January 15, 2021.
Supplementary Information: The FAA issued a notice of proposed rulemaking (NPRM) to amend 14 CFR part 39 by adding an AD that would apply to all SAP Model IO-360-series and O-360-series reciprocating engines and certain Lycoming Model AEIO-360-, IO-360-, and O-360-series reciprocating engines with a certain SAP crankshaft assembly installed. The NPRM published in the Federal Register on January 29, 2020 (85 FR 5173). The NPRM was prompted by three crankshaft assembly failures that resulted in the loss of engine power and immediate or emergency landings. The FAA determined that the crankshaft assembly failures resulted from the manufacturing process at SAP's crankshaft vendor during 2012 and 2014 causing excessive residual white layer of iron nitride forming on the assemblies. This white layer is brittle and can lead to spalling or fatigue cracking of the crankshaft assembly as a result of the normal mechanical loads during engine operation. The FAA's analysis concluded that all three SAP crankshaft
assembly failures were the result of this fatigue cracking. In the NPRM, the FAA proposed to require the removal from service of all affected crankshaft assemblies. The unsafe condition, if not addressed, could result in failure of the engine, in-flight shutdown, and loss of the airplane.
More News
Decision Altitude (DA) A specified altitude (mean sea level (MSL)) on an instrument approach procedure (ILS, GLS, vertically guided RNAV) at which the pilot must decide whether to >[...]
Aero Linx: T-34 Association, Inc. The T-34 Association was formed in July 1975 so that individuals purchasing then military surplus T-34As had an organization which would provide s>[...]
As He Released The Brakes To Begin Taxiing, The Brake Pedals Went To The Floor With No Braking Action Analysis: The pilot reported that during engine start up, he applied the brake>[...]
“Legislation like the Mental Health in Aviation Act is still imperative to hold the FAA accountable for the changes they clearly acknowledge need to be made... We cannot wait>[...]
Also: IAE Acquires Diamond Trainers, Army Drones, FedEx Pilots Warning, DA62 MPP To Dresden Tech Uni The danger to the flight training industry and our future pilots is clear. Dona>[...]