Sat, Nov 11, 2023
Accident Occurred During The Fifth Flight Of The Phase 1 Test Flights
Location: Wasilla, Alaska Accident Number: ANC22FA069
Date & Time: August 29, 2022, 12:04 Local Registration: N2723P
Aircraft: Story Charles Brad TT FOX Aircraft Damage: Substantial
Defining Event: Unknown or undetermined Injuries: 1 Fatal
Flight Conducted Under: Part 91: General aviation - Flight test
![](/images/content/politics/2011/NTSB-Logo-0411b.jpg)
Analysis: According to witnesses, the airplane took off on runway 08 and then turned back toward the airport. The pilot made a radio call that he was turning downwind for landing. The accident occurred during the fifth flight of the phase 1 test flights after the pilot finished building the airplane. Witnesses heard changes in the engine rpm they described as the engine revving, going to idle, and surging. They also reported that the airplane was traveling “fast,” with pitch oscillations; the airplane approached the gravel runway in a right-wing-low turn as if it was going to land. The airplane then pitched down abruptly before striking trees about 60 to 80 ft before penetrating the side of a hangar, where it came to rest.
Data downloaded from an onboard device showed the airplane turned crosswind after takeoff then entered a right downwind for the runway. Once abeam the departure end of the runway, the airplane stopped its climb, began a descent, and turned toward the approach end of the intersecting gravel strip. The data also showed that the engine rpm changed from idle to maximum three times in the last 8 seconds of flight.
Examination of the airplane revealed no mechanical malfunctions or anomalies that would have precluded normal operation. The reason for the rpm oscillations and pitch variations could not be determined with the available information. Given the witness statements and that the pilot was turning toward the gravel runway, it is likely that he was experiencing an issue with the airplane that could not be determined with the available information.
Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s inability to maintain control of the airplane for reasons that could not be determined.
More News
Have A Story That NEEDS To Be Featured On Aero-News? Here’s How To Submit A Story To Our Team Some of the greatest new stories ANN has ever covered have been submitted by our>[...]
“The legislation now includes a task force with industry representation ensuring that we have a seat at the table and our voice will be heard as conversations about the futur>[...]
Aero Linx: Waco Museum The WACO Historical Society, in addition to preserving aviation's past, is also dedicated and actively works to nurture aviation's future through its Learnin>[...]
Adcock Range National low-frequency radio navigation system (c.1930-c.1950) replaced by an omnirange (VOR) system. It consisted of four segmented quadrants broadcasting Morse Code >[...]
Also: uAvionix AV-Link, Does Simming Make Better Pilots?, World Games, AMA National Fun Fly Czech sportplane manufacturer Direct Fly has finished delivering its 200th ALTO NG, the >[...]