NTSB Final Report: Piper PA-36-375 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-10.20.25

AirborneUnlimited-
10.14.25

Airborne-Unlimited-10.15.25

Airborne-NextGen-10.16.25

AirborneUnlimited-10.17.25

Sat, May 10, 2025

NTSB Final Report: Piper PA-36-375

...Added Full Power And Pushed The Propeller Control Full Forward, But Did Not Feel The Engine Respond

Location: Avoca, Nebraska Accident Number: CEN24LA269
Date & Time: July 16, 2024, 14:30 Local Registration: N2386X
Aircraft: Piper PA-36-375 Aircraft Damage: Substantial
Defining Event: Powerplant sys/comp malf/fail Injuries: 1 None
Flight Conducted Under: Part 137: Agricultural

Analysis: The pilot reported that, during an aerial application flight, the engine lost power and the airplane began to descend. He added full power and pushed the propeller control full forward, but did not feel the engine respond and the airplane continued to descend. After he dumped the hopper tank, he still was not able to stop the airplane’s descent, and the airplane touched down in the field and continued through a cattle fence, resulting in substantial damage to the fuselage and left wing.

The airplane was recovered to a secure facility for further examination. There was a crack observed between the Nos. 1, 2, and 3 cylinders that was most likely the result of impact damage. Examination of the magnetos revealed that, while still attached to the engine, the left magneto could be rotated at its flange. Both magnetos were removed and spun by hand and both magnetos produced spark at their terminal leads. The right magneto made a “clunking” sound when rotated and rattled when shaken. Further examination revealed that the right magneto coil wedges were loose in the housing. The coil wedges appeared to have been initially wedged in place, but only exhibited minimal marring, and may not have been secured sufficiently.

That the left magneto was found loose and could be rotated at its flange, it’s likely it was out of time. Although the right magneto coil wedges were loose in the housing, it is more likely the left magneto firing at the wrong time would have had the most significant impact on the engine only being able to produce partial power.

Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- A partial loss of engine power due to the loose left magneto which resulted in erratic engine timing.

FMI: www.ntsb.gov

Advertisement

More News

Airborne 10.15.25: Phantom 3500 Confounds, Citation CJ3 Gen2 TC, True Blue Power

Also: Kodiak 100 Joins USFS, Innovative Solutions & Support Renamed, Gulfstream Selects Honeywell, Special Olympics Airlift The Phantom 3500 mockup made an appearance where the>[...]

Updated: Gryder Arrested On Gun Charge, Cites ‘Georgia Stand Your Ground’ Law

Incidents Allegedly Occured As Described in Police Report(s) 25-005809 and 25-005818 The name ’Dan Gryder’ is fairly well known to many in aviation.... Whether you like>[...]

Aero-News: Quote of the Day (10.18.25)

“Recent U.S. government policy updates emphasizing investment in domestic drone manufacturing align perfectly with our joint venture objectives, positioning us to meet critic>[...]

ANN's Daily Aero-Term (10.18.25): Final Approach Point

Final Approach Point The point, applicable only to a nonprecision approach with no depicted FAF (such as an on airport VOR), where the aircraft is established inbound on the final >[...]

Classic Aero-TV: Eyeing the Hawk

From 2023 (YouTube Edition): The Best of the Eighties in the Early Twenties It can be argued with confidence that the father of the Ultralight aircraft from which the Light-Sport A>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC