NTSB Releases Preliminary Report In Bonanza Accident In Colorado | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-06.23.25

Airborne-NextGen-06.24.25

AirborneUnlimited-06.25.25

Airborne-AffordableFlyers-06.26.25

AirborneUnlimited-06.27.25

Wed, Feb 21, 2018

NTSB Releases Preliminary Report In Bonanza Accident In Colorado

Airplane Experienced A Loss Of Engine Power During Touch-And-Go Landings

The NTSB has released a preliminary report from an accident which occurred January 13, 2018 at about 1715 mountain standard time. A Beech K35 Bonanza, N803R, experienced a loss of engine power after departure from Vance Brand Airport, (KLMO), Longmont, Colorado. The pilot sustained serious injuries, the passenger sustained minor injuries, and the airplane sustained substantial damage. The airplane was registered to and operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed at the time of the accident and no flight plan had been filed. The local flight was departing KLMO at the time of the accident.

A witness reported that he was near taxiway A3 when heard "a popping noise" coming from the accident airplane during takeoff. A few seconds later he heard the engine "shut off" as the airplane was in a nose up attitude. The airplane rolled to the right and then descended in a "steep dive" toward the ground. When he arrived at the accident site (figure 1) he observed smoke and smelled fuel near the airplane. He stated that the ground near the airplane was wet and fuel was leaking from the wing where it had separated from the fuselage.

The airplane owner, who is the father-in-law of the pilot, stated that he spoke with both the pilot and passenger; the passenger did not remember anything except the preflight inspection before the flight began. The pilot told the owner that they returned to KLMO to perform touch-and-go landings. During the climb out, after the second consecutive touch-and-go, the engine lost power, so the pilot pushed the nose down and made a forced landing in a field off the end of the runway. The pilot added that the landing gear had already been retracted and there was no remaining runway available to land.

(Image provided with NTSB preliminary report)

FMI: Report

Advertisement

More News

NTSB Prelim: Piper PA-23

Pilot Also Reported That Due To A Fuel Leak, The Auxiliary Fuel Tanks Were Not Used On June 4, 2025, at 13:41 eastern daylight time, a Piper PA-23, N2109P, was substantially damage>[...]

ANN FAQ: Submit a News Story!

Have A Story That NEEDS To Be Featured On Aero-News? Here’s How To Submit A Story To Our Team Some of the greatest new stories ANN has ever covered have been submitted by our>[...]

Classic Aero-TV: One Man’s Vietnam

From 2023 (YouTube Edition): Reflections on War’s Collective Lessons and Cyclical Nature The exigencies of war ought be colorblind. Inane social-constructs the likes of racis>[...]

ANN's Daily Aero-Linx (07.03.25)

Aero Linx: Colorado Pilots Association (CPA) Colorado Pilots Association was incorporated as a Colorado Nonprofit Corporation in 1972. It is a statewide organization with over 700 >[...]

ANN's Daily Aero-Term (07.03.25): High Speed Taxiway

High Speed Taxiway A long radius taxiway designed and provided with lighting or marking to define the path of aircraft, traveling at high speed (up to 60 knots), from the runway ce>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC