NTSB Prelim: Cirrus Design Corp SR22T | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-SpecialEpisode-12.15.25

AirborneNextGen-
12.16.25

Airborne-Unlimited-12.10.25

Airborne-AffordableFlyers-12.11.25

AirborneUnlimited-12.12.25

AFE 2025 LIVE MOSAIC Town Hall (Archived): www.airborne-live.net

Tue, Sep 03, 2024

NTSB Prelim: Cirrus Design Corp SR22T

Pilot Looked Up And Saw Light White Smoke Coming From Around The Propeller Spinner

Location: Tulsa, OK Incident Number: CEN24LA308
Date & Time: August 3, 2024, 13:00 Local Registration: N825JC
Aircraft: Cirrus Design Corp SR22T Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Ferry

On August 3, 2024, at 1300 central daylight time, a Cirrus SR22T, N825JC, was involved in an incident near Tulsa, Oklahoma. The airplane sustained unknown damage. The pilot was uninjured. The airplane was operated under Title 14 Code of Federal Regulations Part 91 as a ferry flight.

Prior to the ferry flight, an engine was installed onto the airplane by an airframe and powerplant mechanic with inspection authorization. The engine installation also included the installation of Alternator 1 and Alternator 2. The mechanic was not affiliated with a certificated aircraft repair station or Cirrus Aircraft. A runup of the engine was performed by the mechanic, and a maintenance check flight was not performed prior to the ferry flight. The ferry pilot flew the airplane from Tulsa Riverside Airport, Tulsa, Oklahoma, to Tulsa International Airport (TUS), Tulsa, Oklahoma, where the airplane’s parachute was to be repacked. The ferry flight arrived at TUS without incident, where the pilot parked and shutdown the airplane on a fixed base operator ramp. While the pilot was still seated in the airplane, line personnel saw smoke coming from the engine compartment. The pilot looked up and saw light white smoke coming from around the propeller spinner. As the pilot exited the airplane, he saw an increase in smoke and a change in its color to a darker color. The pilot looked into the louvered vents under the engine compartment and saw electrical arching and smoke. The pilot did not see any fire. The pilot called the fire department and sprayed halon through the louvered vents. Line personnel sprayed a dry multipurpose extinguisher into the airplane’s engine oil access door. 

Two fire department trucks then arrived and took control of the scene. Postaccident examination of the airplane revealed that Alternator 1 (Plane Power, model number ES10024, serial number H-X092248) had external wire connections that were not in accordance with Cirrus Airplane Maintenance Manual Models SR22 and SR22T. 

An airplane logbook entry by the mechanic, dated August 10, 2023, at an hour meter of 1,122.4 hours, stated that a rebuilt engine and both alternators were installed. An airplane logbook entry by the mechanic, dated July 22, 2024, at an hour meter of 1,138.1 hours, stated the engine was removed due to a loss of oil pressure, a rebuilt engine was installed, and both alternators were installed.

The airplane battery and associated wiring sustained thermal damage. The airplane was retained for further examination and determination of damage to the firewall.

FMI: www.ntsb.gov

Advertisement

More News

ANN's Daily Aero-Term (12.13.25): Light Gun

Light Gun A handheld directional light signaling device which emits a brilliant narrow beam of white, green, or red light as selected by the tower controller. The color and type of>[...]

Aero-News: Quote of the Day (12.13.25)

“We have performed extensive ground testing by comparing warm up times, full power tethered pulls, and overall temperatures in 100 degree environments against other aircraft >[...]

NTSB Final Report: Gippsland GA-8

While Taxiing To Parking The Right Landing Gear Leg Collapsed, Resulting In Substantial Damage Analysis: The pilot made a normal approach with full flaps and landed on the runway. >[...]

Classic Aero-TV: Historically Unique -- Marlin Horst's Exquisite Fairchild 71

From 2014 (YouTube Edition): Exotic Rebuild Reveals Aerial Work Of Art During EAA AirVenture 2014, ANN's Michael Maya Charles took the time to get a history lesson about a great ai>[...]

Airborne 12.12.25: Global 8000, Korea Pilot Honors, AV-30 Update

Also: Project Talon, McFarlane Acquisition, Sky-Tec Service, JPL Earth Helo Tests Bombardier has earned a round of applause from the business aviation community, celebrating the fo>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2025 Web Development & Design by Pauli Systems, LC