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Tue, Aug 04, 2009

NTSB Determines go! Airline Pilots Fell Asleep In Flight

Captain Later Diagnosed With Sleep Apnea

The NTSB has released a probable cause report for an incident in which both pilots of a go! Airlines Bombardier CL-600 fell asleep while flying from Honolulu to Hilo, Hawaii. While the captain on the flight was later diagnosed with obstructive sleep apnea, the NTSB determined that crew fatigue played a major role in the incident. After overshooting its destination by 26 miles, the plane returned to Hilo and landed safely. The NTSB report says, in part:

Scheduled 14 CFR Part 121: Air Carrier operation of Mesa Airlines (D.B.A. GO)
Incident occurred Wednesday, February 13, 2008 in Hilo, HI
Probable Cause Approval Date: 8/3/2009 3:34:10 PM
Aircraft: Bombardier, Inc. CL-600, registration: N651BR
Injuries: 43 Uninjured

go! flight 1002 departed for its destination about 0916 Hawaii standard time. About 0930, the captain transmitted to air traffic control (ATC) that the flight was climbing through 11,700 feet to its cruise altitude of flight level (FL) 210 (approximately 21,000 feet mean sea level.) The controller acknowledged the transmission and cleared the flight to proceed to an intersection along the flight route located about 29 miles north-northwest of the destination airport, and the flight crew acknowledged. At 0933, during cruise flight, the controller repeated the navigational clearance, which the flight crew acknowledged, and the airplane turned in accordance with the clearance. At 0940, the controller instructed the flight to change radio frequencies, and there was no response. The controller continued to try to contact the flight crew multiple times but received no reply. At 0951, the airplane crossed the intersection that was its clearance limit then turned southeast toward the destination airport without descending, which is consistent with the airplane being on autopilot. The controller handling the flight asked another controller to attempt to contact the flight crew on a different frequency, but there was still no response, and the flight proceeded on a southeasterly heading at FL 210. About 0955, the flight crossed over the destination airport and continued on a southeasterly course without changing altitude or heading. Two separate airline crews in the area attempted to contact the incident crew, but neither flight crews’ attempts were successful.

About 0958, when the flight was about 26 nautical miles southeast of the destination airport, the captain contacted the controller with an abbreviated call sign (“Ah HCF ten zero two”), and the controller asked if the flight crew was experiencing an emergency. The captain responded, "No, we must have missed a hand off or missed a call or something." The controller then issued instructions for the flight to return to the destination airport, with which the flight crew complied. The flight arrived without further incident about 1015.

The captain and first officer both reported to their company that they had unintentionally fallen asleep in flight. The fact that both pilots fell asleep during the midmorning hours, a time of day normally associated with wakefulness and rising alertness, indicates that both pilots were fatigued.

The captain had undiagnosed severe obstructive sleep apnea, which was diagnosed during a medical evaluation shortly after this incident and for which symptoms (such as snoring) and risk factors (such as obesity) were present before the incident. This condition likely caused him to experience chronic daytime fatigue and contributed to his falling asleep during the incident flight.

File Photo

In addition, the day of the incident was the third consecutive day that both pilots started duty at 0540. This likely caused the pilots to receive less daily sleep than is needed to sustain optimal alertness and resulted in an accumulation of sleep debt and increased levels of daytime fatigue. The first officer stated he needed between 7.5 and 8 hours of sleep per night to feel rested. He estimated that he had spent about 7 hours 25 minutes in bed the night before the incident, and about 6 hours 55 minutes in bed during each of the previous two nights. Thus, the first officer’s self-reported sleep history indicated an accumulated sleep debt of between 1 hour 15 minutes and 2 hours 45 minutes in the 72 hours before the incident. The first officer’s reduced sleep probably resulted from the flight crew’s recent work schedule.

The incident pilots’ lack of adequate sleep, together with the low workload associated with the cruise phase of the flight, likely contributed to the pilots inadvertently falling asleep.

The National Transportation Safety Board determines the probable cause(s) of this incident as follows:

The captain and first officer inadvertently falling asleep during the cruise phase of flight. Contributing to the incident were the captain's undiagnosed obstructive sleep apnea and the flight crew’s recent work schedules, which included several consecutive days of early-morning start times.

FMI: www.ntsb.gov

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