NTSB Releases Preliminary Report From PA-46 Ditching In PA | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.22.24

Airborne-Unlimited-04.16.24

Airborne-FlightTraining-04.17.24 Airborne-AffordableFlyers-04.18.24

Airborne-Unlimited-04.19.24

Join Us At 0900ET, Friday, 4/10, for the LIVE Morning Brief.
Watch It LIVE at
www.airborne-live.net

Fri, Nov 01, 2019

NTSB Releases Preliminary Report From PA-46 Ditching In PA

Pilot Said Airplane Lost Power On Approach To Harrisburg International Airport

The NTSB has released a preliminary report from an accident which occurred on October 4 involving a Piper PA46-310P which was involved in a forced landing in the Susquehanna River.

According to the report, the airplane lost engine power while on approach to the Harrisburg International Airport (KMDT), Harrisburg, Pennsylvania. The private pilot and a passenger sustained minor injuries. Visual meteorological conditions prevailed, and an instrument flight rules (IFR) flight plan was filed for the personal flight which originated at the Greater Rochester International Airport (KROC), about 1600.

In a written statement, the pilot stated he conducted a "thorough" preflight inspection and had the airplane serviced with 30 gallons of 100LL gasoline. He estimated that the 122-gallon fuel system contained 77 gallons of fuel at departure.

The pilot described the flight as "unremarkable." He said that he flew an extended right downwind leg of the traffic pattern, turned and intercepted the final approach course, and was cleared for the visual approach to runway 31 by the MDT tower controller. The pilot said he referenced the course and glideslope indications for the instrument landing system ILS RWY 31 approach during the descent.

According to the pilot, "I had the ILS loaded and was tracking the final approach course and glide slope as I dropped the gear. I added the first notch of flaps and the engine cut out. I pitched for best glide speed as I tried to restart the engine, advanced the power, and switched fuel tanks, none of which worked. We were losing altitude quickly. I retracted the gear and prepared for a water landing. I advised the tower that we were not going to make the runway. I would estimate that we touched down 1-2 miles from the runway."

The pilot held a private pilot certificate with ratings for airplane single engine land and instrument airplane. His most recent FAA third class medical certificate was issued June 10, 2019. The pilot reported 1,502 total hours of flight experience, of which 433 hours were in the accident airplane make and model.

According to FAA records, the airplane was manufactured in 1984 and was powered by a Continental TSIO 550C 310-horsepower engine. Its most recent annual inspection was completed March 1, 2019 at 5,085 total aircraft hours, and the airplane had accrued 20 hours since that date.

The engine had accrued 2,381.7 hours of total time, of which 74.7 hours were since major overhaul.

Examination of the wreckage revealed the airplane was intact, but that the fuselage was deformed aft of the cabin door. Both wings were cut at their roots by recovery personnel. Prior to removal of the wings, each wing was drained of fuel and water. The left wing contained 12.5 gallons of fuel and 10 gallons of water. The right wing contained 17 gallons of fuel and 15 gallons of water.

Flight control continuity was confirmed from the flight controls to all flight control surfaces. Fuel system continuity was confirmed from the roots of each wing to the fuel metering unit. Electrical power was applied to the fuel boost pumps in each wing, and both operated when energized.

The engine spark plugs were removed from the top of each cylinder. Each spark plug displayed normal wear and evidence of exposure to water. The engine was rotated by hand at the propeller; both magneto impulse couplings "snapped," and spark was produced at the ignition leads of the top six spark plugs.

The engine retained for further examination.

(Source: NTSB. Image from file. Not accident airplane)

FMI: Report

Advertisement

More News

ANN's Daily Aero-Term (04.24.24): Runway Lead-in Light System

Runway Lead-in Light System Runway Lead-in Light System Consists of one or more series of flashing lights installed at or near ground level that provides positive visual guidance a>[...]

ANN's Daily Aero-Linx (04.24.24)

Aero Linx: Aviation Without Borders Aviation Without Borders uses its aviation expertise, contacts and partnerships to enable support for children and their families – at hom>[...]

Aero-FAQ: Dave Juwel's Aviation Marketing Stories -- ITBOA BNITBOB

Dave Juwel's Aviation Marketing Stories ITBOA BNITBOB ... what does that mean? It's not gibberish, it's a lengthy acronym for "In The Business Of Aviation ... But Not In The Busine>[...]

Classic Aero-TV: Best Seat in The House -- 'Inside' The AeroShell Aerobatic Team

From 2010 (YouTube Version): Yeah.... This IS A Really Cool Job When ANN's Nathan Cremisino took over the lead of our Aero-TV teams, he knew he was in for some extra work and a lot>[...]

Airborne Affordable Flyers 04.18.24: CarbonCub UL, Fisher, Affordable Flyer Expo

Also: Junkers A50 Heritage, Montaer Grows, Dynon-Advance Flight Systems, Vans' Latest Officially, the Carbon Cub UL and Rotax 916 iS is now in its 'market survey development phase'>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC