NTSB: Downed Blimp Unable To Outrun Storm | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.29.24

Airborne-NextGen-04.30.24

Airborne-Unlimited-05.01.24 Airborne-AffordableFlyers--05.02.24

Airborne-Unlimited-05.03.24

Sun, Jul 10, 2005

NTSB: Downed Blimp Unable To Outrun Storm

Investigation Continues

The NTSB released the factual report this week about the crash of a Goodyear blimp in Coral Springs. The report quotes the pilot saying that the blimp was "unable to climb, make headway, or maintain directional control" with the engines at full power once caught in the storm.

The 192-foot-long gray, blue and yellow Stars and Stripes blimp crashed into an industrial park on June 16th after the pilot attempted to escape the storm.

The pilot had left the Pompano Beach Airpark about 1530 in good weather with scattered showers. He took the blimp south towards Miami Beach. About 1630, he started back for to the airport.

By 1725, the weather was worsening and showers were approaching the airport. While on approach, the pilot said that he saw several cloud-to-ground lightning strikes within a mile of the base. With the safety of the ground crew in mind, he decided to attempt to leave the area and wait out the storms.

Unfortunately, Mother Nature didn't cooperate, and the airship was "being pushed backward and down" even while the pilot was attempting to climb with full power. The heavy rain, lightning and "severe outflow and downdrafts" forced the aircraft down.

While the pilot attempted to steer away from homes, the blimp struck trees and powerlines while coming to rest top of a mini storage facility and several cars, vans, and trailers. The impact tore the helium-filled envelope and damaged the right propeller and lower fin of the craft.

The pilot, Daniel Thomas, 43, and passenger Charles Thomas, 48,were not injured.

FMI: www.goodyearblimp.com, www.ntsb.gov

Advertisement

More News

ANN's Daily Aero-Linx (05.02.24)

Aero Linx: Model Aeronautical Association of Australia MAAA clubs are about fun flying, camaraderie and community. For over 75 years, the MAAA has been Australia’s largest fl>[...]

ANN's Daily Aero-Term (05.02.24): Touchdown Zone Lighting

Touchdown Zone Lighting Two rows of transverse light bars located symmetrically about the runway centerline normally at 100 foot intervals. The basic system extends 3,000 feet alon>[...]

Aero-News: Quote of the Day (05.02.24)

“Discovery and innovation are central to our mission at Virgin Galactic. We’re excited to build on our successful record of facilitating scientific experiments in subor>[...]

ANN FAQ: Contributing To Aero-TV

How To Get A Story On Aero-TV News/Feature Programming How do I submit a story idea or lead to Aero-TV? If you would like to submit a story idea or lead, please contact Jim Campbel>[...]

NTSB Final Report: Cirrus Design Corp SR20

Student Pilot Reported That During Rotation, “All Of A Sudden The Back Of The Plane Kicked To The Right..." Analysis: The student pilot reported that during rotation, “>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC