NTSB Prelim: Cessna 140 | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.29.24

Airborne-Unlimited-04.23.24

Airborne-Unlimited-04.24.24 Airborne-FltTraining-04.25.24

Airborne-Unlimited-04.26.24

Sun, Aug 09, 2020

NTSB Prelim: Cessna 140

About 2 Minutes Into The Flight, The Engine Started To Run A "Little Bit Rough And Shaky"

Location: Arlington, TX Accident Number: CEN20LA291
Date & Time: 07/18/2020, 0745 CDT Registration: N140AB
Aircraft: CESSNA 140 Injuries: 2 None
Flight Conducted Under: Part 91: General Aviation - Instructional

On July 18, 2020, about 0745 central daylight time, a Cessna 140 airplane, N140AB, was substantially damaged when it was involved in an accident near Arlington, Texas. The flight instructor and student pilot were uninjured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the flight instructor, the purpose of this flight was to fly the airplane crosscountry for tire repairs, and at the same time, to train the student pilot on the airplane. The student pilot started the engine about 0715. The recorded weather indicated the temperature was 26° C and the dew point was 23° C. The flight instructor mentioned that since the outside air temperature was close to the dew point, they would have to be careful and cautious about
carburetor icing, even if there was no visible moisture in the air.

The flight instructor related a previous occurrence when he flew this airplane for the first time with another instructor. The condition was almost 100% relative humidity and the carburetor heat was kept on about "10%" during the flight when at cruise power setting and full carburetor heat at lower than cruise power. However, a rough engine or any sign of carburetor ice was not encountered during that flight.

During the accident flight, the airplane's engine performed as expected during the run up. The student pilot set the carburetor heat on cold for takeoff and departed without issues. The flaps were retracted and the airplane was accelerated to best climb airspeed. The rate of climb was about 250 ft per minute and the engine was running at full power.

About 2 minutes into the flight, the engine started to run a "little bit rough and shaky." The instructor pulled the carburetor heat on about 10% hot and left it in this position in accordance with his training for this airplane. The engine roughness disappeared, and the airplane kept climbing at the same rate.

About 1 minute after this event, the roughness came back more severe this time. The instructor pulled the carburetor heat all the way on to full hot and waited. The roughness continued and the power available was not allowing the airplane to continue the climb at the same rate.

The airplane's pitch attitude was progressively lowered to maintain the airspeed and full power was not sufficient to keep the level flight attitude at 1,200 ft. There was no suitable area ahead for about the next 8 to 10 miles to perform an off-field emergency landing.

The instructor elected to turn back to the departure airport. He was not confident that the airplane could maintain altitude in the traffic pattern, so he elected to conduct a landing on a closer runway with a quartering tailwind. During the landing roll, as the airplane slowed down, he retracted the flaps to remove any residual lift and applied the yoke "slightly diving" away from the wind. While the airplane was still moving forward at a low ground speed, the nose "suddenly" yawed very "quickly and strongly" to the right. Application of the ailerons, elevators, and full left rudder and full left brake did not remedy the yaw. The airplane subsequently ground looped and came to rest in the grass.

Using the pilot's reported departure weather, the plotted relative humidity at this temperature and dewpoint spread was about 80%. Review of the icing probability chart contained in Federal Aviation Administration Special Airworthiness Information Bulletin CE-09-35 revealed that the weather conditions at the time of the accident were "conducive to serious icing at glide power."

The operator of the airplane was asked to run the engine after the accident. The engine started and operated "normally."

FMI: www.ntsb.gov

Advertisement

More News

ANN's Daily Aero-Term (04.28.24): Airport Marking Aids

Airport Marking Aids Markings used on runway and taxiway surfaces to identify a specific runway, a runway threshold, a centerline, a hold line, etc. A runway should be marked in ac>[...]

Aero-News: Quote of the Day (04.28.24)

"It is extremely difficult, if not impossible, for manned aircraft to see a drone while conducting crop-enhancing and other aerial applications at low altitudes and high speeds. We>[...]

ANN's Daily Aero-Linx (04.28.24)

Aero Linx: The Skyhawk Association The Skyhawk Association is a non-profit organization founded by former Skyhawk Pilots which is open to anyone with an affinity for the A-4 Skyhaw>[...]

Aero-News: Quote of the Day (04.29.24)

“The T-54A benefits from an active Beechcraft King Air assembly line in Wichita, Kansas, where all required METS avionics and interior modifications are installed on the line>[...]

ANN's Daily Aero-Linx (04.29.24)

Aero Linx: Aerostar Owners Association The Association offers the Aerostar Owner a unique opportunity to tap an invaluable source of information concerning the care and feeding of >[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC