NTSB Prelim: Cirrus Design Corp SR22T | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-05.13.24

Airborne-NextGen-05.07.24

Airborne-Unlimited-05.08.24 Airborne-FlightTraining-05.09.24

Airborne-Unlimited-05.10.24

Sun, Mar 24, 2024

NTSB Prelim: Cirrus Design Corp SR22T

Engine RPM Surged A Few Times, Followed By The Sound Of A Loud Bang And Subsequent Total Loss Of Engine Power

Location: Bellevue, WA Incident Number: WPR24FA103
Date & Time: March 5, 2024, 17:04 Local Registration: N927CS
Aircraft: Cirrus Design Corp SR22T Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Instructional

On March 5, 2024, about 1704 Pacific standard time, a Cirrus SR-22T, N927CS, sustained minor damage when it was involved in an incident near Bellevue, Washington. The flight instructor and the pilot receiving instruction were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight. The flight instructor and pilot receiving instruction reported that after takeoff from runway 34, Renton Municipal Airport, they leveled off at about 2,500 ft mean sea level (msl). A few minutes later, the engine RPM surged a few times, followed by the sound of a loud bang and subsequent total loss of engine power. Unable to restart the engine, they deployed the Cirrus Airframe Parachute System (CAPS), and the airplane descended under the parachute into a wooded wetland area adjacent to a residential neighborhood.

Examination of the incident site revealed that the airplane impacted terrain about 4 miles northeast of the departure end of runway 34. The airplane came to rest upright in an approximate 10° nose low attitude, on a heading of about 066° magnetic, at an elevation of about 417 ft msl.

The wreckage was recovered to a secure location for further examination. Review of the airframe and engine logbooks revealed that the engine, a Continental Motors TSIO-550-K1B, was overhauled in November 2019 and installed on the airframe in April 2020. At the time of the incident, the engine had accumulated about 680 hours since major overhaul. 

FMI: www.ntsb.gov

Advertisement

More News

Airborne 05.10.24: Icon Auction, Drunk MedEvac Pilot, Bell ALFA

Also: SkyReach Parts Support, Piper Service Ctr, Airliner Near-Miss, Airshow London The Judge overseeing Icon's convoluted Chapter 11 process has approved $9 million in Chapter 11 >[...]

ANN's Daily Aero-Term (05.13.24): ILS PRM Approach

ILS PRM Approach An instrument landing system (ILS) approach conducted to parallel runways whose extended centerlines are separated by less than 4,300 feet and at least 3,000 feet >[...]

ANN's Daily Aero-Linx (05.13.24)

Aero Linx: FlyPups FlyPups transports dogs from desperate situations to fosters, no-kill shelters, and fur-ever homes. We deliver trained dogs to veterans for service and companion>[...]

Airborne-NextGen 05.07.24: AI-Piloted F-16, AgEagle, 1st 2 WorldView Sats

Also: Skydio Chief, Uncle Sam Sues, Dash 7 magniX, OR UAS Accelerator US Secretary of the Air Force Frank Kendall was given a turn around the patch in the 'X-62A Variable In-flight>[...]

Airborne 05.08.24: Denali Update, Dad-Daughter Gyro, Lake SAIB

Also: NBAA on FAA Reauth, DJI AG Drones, HI Insurance Bill Defeated, SPSA Airtankers The Beechcraft Denali continues moving forward towards certification, having received its FAA T>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC