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NTSB Released Prelim In Fatal Bellanca Accident

Pilot Fatally Injured, Three Passengers Survived

The NTSB has released a preliminary report from a November 30th accident that resulted in the fatal injury of the commercially-rated pilot of a Bellanca model 17-30 airplane. The three others on board the aircraft survived with serious injuries.

According to the report, on November 30 at about 0900 central standard time, the airplane was substantially damaged when it collided with terrain during landing approach to runway 36 at Jesse Viertel Memorial Airport (KVER), Boonville, MO.

The airplane was registered to and operated by the pilot. Day visual meteorological conditions prevailed for the cross-country flight that departed Spirit of St. Louis Airport (KSUS), Chesterfield, Missouri, about 0738, and was originally destined for Charles B. Wheeler Downtown Airport (KMKC), Kansas City, Missouri.

The day before the accident, the pilot had flown from KMKC to KSUS. After landing, about 1207, the pilot told a fixed-base operator (FBO) line technician that he had a depleted battery because of an unspecified charging system malfunction. The pilot, who also was an aviation mechanic, removed the battery from the airplane to have it charged. About 1800, the pilot returned to the FBO with the recharged battery. After reinstalling the battery, the pilot started and ran the engine for about 5 to 7 minutes. Following the engine run, the pilot removed the cowling and began adjusting a subcomponent of the alternator control unit (ACU). After adjusting the ACU, the pilot performed another engine test run that lasted about 10 minutes.

Following the second engine test run, the pilot told the FBO line technician that the airplane's ammeter was still showing a slight discharge while the engine was running, and that he was uncomfortable departing at night with a charging system issue. The pilot asked if he and his passengers could stay the night in the pilot's lounge so they could depart early the following morning. The pilot also asked for the airplane to be towed to the self-serve fuel pumps because he didn't want to further deplete the battery with another engine start.

The pilot prepaid for 20 gallons of fuel at the self-serve fuel pump. According to the line technician, the pilot nearly topped-off the right inboard fuel tank with 13 gallons before switching over to the left inboard tank. Upon a visual inspection of the left inboard tank, the pilot told the line technician that it contained less fuel than he had expected. The pilot proceeded to add the remaining 7 gallons of the prepaid 20 gallons to the left inboard fuel tank. The line technician noted that after fueling the left inboard fuel tank, the fluid level was about 2 inches from the top of the tank. The pilot did not purchase any additional fuel and told the line technician that both outboard "auxiliary" fuel tanks were nearly full. The line technician then towed the airplane back to the ramp for the evening. The line technician reported that the airplane departed FBO ramp the following morning.

According to one of the surviving passengers, while enroute at an altitude of 2,000 to 3,000 feet mean sea level, the flight encountered a line of "dense clouds" near Sedalia, Missouri. The pilot attempted to navigate beneath the clouds, at an altitude of about 1,500 feet msl, before deciding to make a course reversal and locate a nearby airport to divert to. The pilot told the passenger, who was seated in the forward-right seat, to be on the lookout for towers and obstructions because of their low proximity to the ground. The passenger reported that after flying east for a few minutes the pilot identified VER on his tablet computer. The flight approached the airport traffic pattern from the west and made a left base-to-final turn toward runway 36. The passenger reported that the pilot extended the landing gear without any difficulties. However, when the pilot reduced engine power, in attempt to reduce airspeed, the engine experienced a loss of power. The pilot was able to briefly restore engine power by advancing the throttle, but the engine quickly lost total power. The passenger reported that the pilot then began making rapid changes to the engine throttle and mixture control without any noticeable effect to engine operation. The passenger stated that the airplane eventually "stalled completely", about 250 feet above the ground, as the pilot prepared for a forced landing; however, the passenger did not recall the airplane impacting terrain.

A postaccident examination revealed that the airplane impacted a harvested soybean field on a 305 degree magnetic heading. The initial point of impact consisted of three parallel depressions in the field that were consistent with the spacing of the accident airplane landing gear. The main wreckage was located about 24 feet from the initial point of impact in an upright position. The accident site was situated along the extended runway 36 centerline, about 0.4 miles south of the runway approach threshold. Flight control continuity was confirmed from the cockpit controls to the individual flight control surfaces. The electric master switch was found in the "on" position. The wing flaps were observed to be positioned about 1/2 of their full deflection. The landing gear selector switch was in the "down" position; however, all three landing gear assemblies had collapsed during the accident. The main fuel selector was found in the "off" position; however, a first responder had moved the fuel selector from the "auxiliary" position to the "off" position during rescue efforts. The first responder also turned the engine magneto/ignition key to "off" and disconnected the battery terminals after hearing the sound of an electric motor located under the floorboards. (The sound of an electric motor was later identified to be the electrohydraulic motor for the landing gear extension/retraction system.) The auxiliary fuel tank selector was found positioned to the "right" auxiliary wing tank. (The auxiliary fuel tank selector had two positions, "right auxiliary" or "left auxiliary.") The electric fuel pump switch was found in the "off" position. There were no anomalies identified during functional tests of the electric fuel pump and the aerodynamic stall warning system.

The airplane was equipped with two inboard "main" fuel tanks and two outboard "auxiliary" fuel tanks. The reported capacity of each inboard fuel tank was 19 gallons, of which 15.5 gallons were useable per tank. The left inboard tank contained about 5 gallons of fuel. The right inboard tank contained 3-1/2 pints of fuel. The inboard fuel tanks appeared to be undamaged and there was no evidence of a fuel leak from either tank. The reported capacity of each outboard "auxiliary" fuel tank was 17 gallons; however, those tanks were placarded for level flight only. The outboard fuel tanks also appeared to be undamaged and there was no evidence of a fuel leak from either tank. A visual inspection of the left outboard tank confirmed that it was filled near its capacity. The right outboard tank contained about 11 gallons of fuel. No fuel was recovered from the fuel supply line connected to the engine-driven fuel pump inlet port; however, the fuel gascolator drain had fractured during the accident and there was evidence of a small fuel spill underneath the gascolator assembly at the accident site. Only trace amounts of fuel were recovered from the engine-driven fuel pump outflow fuel line. No fuel was recovered from the fuel supply line connected to the flow-divider assembly.

The engine remained partially attached to the firewall by its engine mounts and control cables. Internal engine and valve train continuity was confirmed as the engine crankshaft was rotated. Compression and suction were noted on all cylinders in conjunction with crankshaft rotation. The upper spark plugs were removed and exhibited features consistent with normal engine operation. Both magnetos provided spark on all leads when rotated. There were no obstructions between the air filter housing and the fuel control unit. Mechanical continuity was confirmed from the engine components to their respective cockpit engine controls. The postaccident examination revealed no evidence of mechanical malfunctions or failures that would have precluded normal engine operation.

According to FAA air traffic control data, the accident flight departed SUS around 0738. According to local law enforcement, the initial 911-emergency call was received at 0901. As such, the accident flight, from takeoff to the accident, was at least 1 hour 22 minutes in duration. According to the airplane's owner manual, the expected fuel consumption rate at 2,500 feet msl and 77-percent power was 16.1 gallons per hour. At 77-percent engine power, the accident flight would have consumed at least 22 gallons of fuel; however, engine operation above 77-percent power and/or insufficient leaning would have consumed additional fuel.

At 0855, the VER automated surface observing system reported: wind 310 degrees at 13 knots, gusting 16 knots; broken cloud ceilings at 2,600 feet above ground level (agl) and 3,400 feet agl, overcast ceiling at 4,100 feet agl; 10 mile surface visibility; temperature 11 degrees Celsius; dew point 7 degrees Celsius; and an altimeter setting of 29.82 inches of mercury.

(Image from file. Not accident airplane)

FMI: www.ntsb.gov

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