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NTSB Releases Factual Report In 2012 VA Helo Accident

Bell 407 Went Down In A Lake Resulting In Pilot's Fatal Injury

The NTSB has released a factual report detailing an accident that occurred August 24, 2012 near Abingdon, VA. The accident fatally injured the Airline Transport-rated pilot of the Bell 407 that impacted the water at South Holston Lake on a personal flight.

According to the report, the accident occurred at about 2230 eastern daylight time. The Bell 407 helicopter, N407N, collided into the lake during a night departure from a river bank in Abingdon, Virginia. The helicopter was substantially damaged when it impacted the water. The helicopter was registered to and operated by K-VA-T&W-L Aviation LLC under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual night meteorological conditions prevailed, and no flight plan was filed. The flight was originating from a private field at the time of the accident.

According to a witness, while boating on the lake across from the helicopter landing zone, he watched as the helicopter came in and landed. He recalled that the landing light was on, and he watched as the passengers exited the helicopter. The helicopter then lifted and turned toward the lake, descended down an embankment and made a turn over the lake. The witness said that he noticed that the landing light was not on during the departure flight. The helicopter traveled approximately 150 yards when the bottom skids began to make the water spray on the side of the helicopter. The helicopter then nosed over and made a loud splash. The witness waited for a short moment and then turned on his spot light and moved towards the position of the helicopter. As he moved towards the helicopter, his boat bumped into the tail boom, which was floating away from the fuselage. He continued towards the helicopter and came upon the helicopter floating upside down with the skids upright approximately 2 feet above the water. The witness shined his light throughout the cabin and cockpit but did not see anyone.

The pilot, age 64, held an airline transport pilot certificate for airplane single-engine land, multi-engine land, and rotorcraft-helicopter issued May 27, 2008, and a second-class airman medical certificate issued February 17, 2012, with limitations for corrective lenses. The pilot's logbook was not recovered for review. According to FAA records, the pilot reported 26,000 flight hours on his last medical.

A review of the pilot's flight schedule for that day revealed that the pilot started the passenger flights at 1500 on the day of the accident. A review of the flight schedule times revealed that 10 passenger flights between Bristol Speedway to a private residence near South Holston Lake were made in a period of 1 hour and 20 minutes. After the pilot returned, he was informed that the next flight would start at 2100. During the flights, the pilot hot fueled at the landing site adjacent to the residence where he dropped off and picked up passengers. There is no record of the amount of fuel taken onboard the helicopter during the day. According to the wife of the pilot, he was well rested the night before and there was nothing abnormal about the day. She went on to say that the pilot was in good health.

The seven-seat, skid equipped helicopter, serial number 53077, was manufactured in 1996. It was powered by a Rolls-Royce model 250-C47B turbo-shaft 650-hp engine.

Review of copies of maintenance logbook records showed an annual inspection was completed March 20, 2012, at a recorded airframe total time of 2,339.1 hours, and an engine time of 2,091.0 hours. The Hobbs hour-meter showed 2,427.8 hours at the accident site. The engine control unit recorded an engine total time of 2,771.06.

Video footage from a security camera captured several daytime departures by the pilot earlier that day. In all the takeoffs, the helicopter was low enough to the surface of the lake to allow the main rotor to create a wake on the surface of the water. On the night of the accident, video footage showed the helicopter's anti-collision lights reflecting off of the lake's surface prior to the accident.

The intended landing site was in the backyard at the private residence of the owner of the helicopter, which is an area of turf grass. The landing site was elevated approximately 30 feet above the lake surface. The area is unlit and not a dedicated helipad and it was used frequently by the owner for helicopter operations.

A review of recorded data from the Virginia Highlands Airport, Abingdon, Virginia (VJI) automated weather observation station, elevation 2,087 feet, revealed that at 2235, conditions were wind 100 degrees at 4 knots, visibility of 10 miles, cloud conditions scattered at 11,000 feet above ground level (agl).

The fuselage of the helicopter was recovered on August 28, 2012, approximately 100 yards from the estimated location of the helicopter's original impact point on the water. The helicopter's engine was torn from the fuselage and could not be located due to poor visibility in the water and the irregular bottom features which rendered the search ineffective.

Examination of the cockpit area of the fuselage revealed that it had been breached during impact. The pilot and copilot's seat pans were broken away from their respective bases and deformed. The instrument panel was dislodged from its mount and held to the fuselage by wiring. A cursory examination of the instrument panel revealed that the landing light switch was found in the "both" position but the landing light circuit breaker was observed in the "out" position (turned off). Examination of the fuselage exhibited evidence of main rotor contact. The top Plexiglas window and frame exhibited evidence of main rotor contact.

Examination of the flight controls revealed that all controls from the collective and cyclic to the vertical control tubes to the hydraulic actuators to the swash plate were intact and no notable damage was observed. The forward vertical firewall exhibited rotational witness marks from the engine to transmission shaft. Rotational witness marks were also present on the transmission shaft. The forward end of the transmission shaft remained attached to the main transmission; the K-Flex coupling on the aft end of the transmission shaft had failed in overload and was splayed outward. The main rotor mast had fractured in overload at its base but had not separated. Examination of the main transmission chip detector upper and lower was found clean of debris. The hydraulic reservoir was found full of hydraulic fluid and clean of debris.

Examination of the main rotor blades revealed that all four rotor blades were fractured consistent with a sudden stoppage. The blue, red, and green pitch change links were bent; the orange pitch change link was fractured in overload. All pitch link hardware was present, and all cotter keys were installed.

The tail boom was fractured at the aft bulkhead and the fracture surfaces were consistent with a main rotor strike. Strike marks were present on both of the top of the vertical stabilizers above the tail boom and the bottom of the vertical stabilizers below the tail boom. The foreword-most 4 feet of the tail boom was not recovered. The vertical fin was not damaged, and the anti-collision light remained intact. The tail boom drive shaft was fractured at the number 3 coupling. Examination of the 90-degree gearbox revealed that the chip detector was found clean and free of debris. The 90-degree gearbox rotated with no binding or grinding. Control continuity was confirmed from the forward fracture to the tail rotor control lever upper end. The tail rotor control lever attachment point showed signs of impact damage and remnants of the arm bearing were located in the lower end of the tail cone. No anomalies were found with the tail rotor which would have prevented normal operation and control.

The engine bay showed evidence of contact by the main rotor. The mounts, engine controls, fuel, oil and electrical connections were all severed from the helicopter. The only engine components present were the Engine Control Unit (ECU), part of a throttle control arm, and a small fragment of the starter/generator mount. All engine mounts were fractured in overload and deformed. The engine oil reservoir, oil cooler, and fan were missing.

Due to extensive impact damage, control continuity could not be established from the cockpit to the engine bay. The collective was fractured at its base. The throttle twist grip was deformed and not movable by hand. The throttle was found in the full-open (fly) position. A piece of the throttle engine's throttle arm was present in the engine bay, still attached to a deformed section of throttle control linkage. The airframe-mounted fuel filter was present. The outlet fuel line to the engine had been severed, allowing water contamination of the filter bowl. The filter bowl was opened and examined. A small amount of silt was present, from the river bed but the filter was otherwise normal. The ECU baseplate was deformed due to impact damage.

An autopsy was performed on the pilot on August 28, 2012, by the Department of Health, Office of the Chief Medical Examiner, Roanoke, Virginia, as authorized by the medical examiner for Washington County. The FAA's Civil Aerospace Medical Institute performed forensic toxicology on specimens from the pilot with negative results for drugs and alcohol.

Examination of the recorded ECU data revealed that there were no engine operating exceedance prior to impact, and no accumulated engine faults were recorded during the previous engine run. No Incident recorder (IR) data had been written to file; however, a partial Snapshot trigger dataset had been recorded. The Snapshot trigger was caused by an Engine Torque Exceedance of 116%. Only seven sequential engine parameters were recorded in the Snapshot data. This is consistent with destruction of the helicopter occurring almost immediately after the initial over-torque event occurred. Electrical power was lost to the ECU before a full line of Snapshot data could be written or any IR data could be recorded.

Due to the limited amount of data recorded on the ECU, very little analysis of engine performance could be achieved. The disparity between main rotor rpm (Nr) and power turbine speed (Np) is attributable to the rapid deceleration of the main rotor as it impacted the water. There is a 24 millisecond cycle time for the data write; however, the Nr signal first passes through a digital converter before the Np signal. During a rapid deceleration of the main rotor, the recorded value for Np will be lower than that recorded for Nr. The recorded Nr data was sampled a few milliseconds before the recorded Np data. The Np data was recorded during or immediately following the main rotor strike of the water.

FMI: www.ntsb.gov

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